石油化工自动化
石油化工自動化
석유화공자동화
AUTOMATION IN PETRO-CHEMICAL INDUSTRY
2011年
6期
54-58
,共5页
曹生伟%逯敬一%曹爱娟%刘炜%术阿杰%张恒伟%岳森
曹生偉%逯敬一%曹愛娟%劉煒%術阿傑%張恆偉%嶽森
조생위%록경일%조애연%류위%술아걸%장항위%악삼
N-甲基二乙醇胺%过滤%闪蒸%蒸汽
N-甲基二乙醇胺%過濾%閃蒸%蒸汽
N-갑기이을순알%과려%섬증%증기
N-methyl-di-ethanolamine%filtrate%flash distillation%steam
高含硫净化装置在运行过程中,N-甲基二乙醇胺(MDEA)溶液发泡问题变得尤为突出,该工况容易造成装旨后路气相带液,严重时会引起冲塔。通过观察装置运行参数,判断总结出MDEA发泡的主要依据是吸收塔的压差上升。结合现场实际操作,发现引起MDEA溶液发泡是各种问题多样化的结果,分别给出解决MDEA溶液系统发泡问题的技术方案。通过对联合装置加入阻泡剂、清洗过滤系统机械过滤器、及时更换活性炭过滤器的活性炭、调整重沸器蒸汽入口的温度等,减小了胺液发泡造成的生产波动及胺液的跑损,实现了除去胺液的杂质和减少胺液降解等目标,得出了详尽的实验数据。数据分析表明该方案取得了较好的生产效果,达到了降耗目的。
高含硫淨化裝置在運行過程中,N-甲基二乙醇胺(MDEA)溶液髮泡問題變得尤為突齣,該工況容易造成裝旨後路氣相帶液,嚴重時會引起遲塔。通過觀察裝置運行參數,判斷總結齣MDEA髮泡的主要依據是吸收塔的壓差上升。結閤現場實際操作,髮現引起MDEA溶液髮泡是各種問題多樣化的結果,分彆給齣解決MDEA溶液繫統髮泡問題的技術方案。通過對聯閤裝置加入阻泡劑、清洗過濾繫統機械過濾器、及時更換活性炭過濾器的活性炭、調整重沸器蒸汽入口的溫度等,減小瞭胺液髮泡造成的生產波動及胺液的跑損,實現瞭除去胺液的雜質和減少胺液降解等目標,得齣瞭詳儘的實驗數據。數據分析錶明該方案取得瞭較好的生產效果,達到瞭降耗目的。
고함류정화장치재운행과정중,N-갑기이을순알(MDEA)용액발포문제변득우위돌출,해공황용역조성장지후로기상대액,엄중시회인기충탑。통과관찰장치운행삼수,판단총결출MDEA발포적주요의거시흡수탑적압차상승。결합현장실제조작,발현인기MDEA용액발포시각충문제다양화적결과,분별급출해결MDEA용액계통발포문제적기술방안。통과대연합장치가입조포제、청세과려계통궤계과려기、급시경환활성탄과려기적활성탄、조정중비기증기입구적온도등,감소료알액발포조성적생산파동급알액적포손,실현료제거알액적잡질화감소알액강해등목표,득출료상진적실험수거。수거분석표명해방안취득료교호적생산효과,체도료강모목적。
During operation process of high sulfur purification device, the foaming problem of N-methyl diethanolamine (MDEA) solution becomes more serious; it can easily cause the gas phase to carry over liquid into later pipeline in the device, and even can cause the tower bumping violently under serious condition. Based on review of operational parameters, it is drawn that MDEA foam is mainly caused by differential pressure increase in absorption tower. Combined with site actual operation, the cause of MDEA solution foaming is found to be combination of variety of problems. Technology scheme for MDEA solution system problem of foaming is put forward. By adding anti-foam agent to combined device, cleaning mechanical filter in filtration system, and timely replacing activate carbon in activated carbon filter, adjusting steam inlet temperature of re-boiler, the target of reduction of production fluctuation and amine liquid loss caused by amine foaming, removing impurities in amine liquid, and reduction of amine degradation are achieved, and detailed experimental data are obtained. Data analysis shows that good production result is achieved with the methods.