化肥设计
化肥設計
화비설계
CHEMICAL FERTILIZER DESIGN
2011年
4期
53-55
,共3页
合成氨装置%中压汽提塔%冷凝液氨回收%加压泵问题%措施
閤成氨裝置%中壓汽提塔%冷凝液氨迴收%加壓泵問題%措施
합성안장치%중압기제탑%냉응액안회수%가압빙문제%조시
ammonia synthesis plant%middle pressure stripper%ammonia recovery from condensate%pressurizing pump%problems%measures
介绍了中压汽提塔冷凝液氨回收的工艺流程、主要设备;分析了试车和生产运行中出现加压泵气化、冷凝液换热器封头泄漏、中压汽提塔塔盘脱落等问题的原因;提出了加压泵壳体上增设排气阀、冷凝液换热器封头垫片表面整体镀银、中压汽提塔塔盘加防转片等项改造措施;结果表明:通过技术改造冷凝液可作为脱盐水利用,合成氨产量增加2 t/d。
介紹瞭中壓汽提塔冷凝液氨迴收的工藝流程、主要設備;分析瞭試車和生產運行中齣現加壓泵氣化、冷凝液換熱器封頭洩漏、中壓汽提塔塔盤脫落等問題的原因;提齣瞭加壓泵殼體上增設排氣閥、冷凝液換熱器封頭墊片錶麵整體鍍銀、中壓汽提塔塔盤加防轉片等項改造措施;結果錶明:通過技術改造冷凝液可作為脫鹽水利用,閤成氨產量增加2 t/d。
개소료중압기제탑냉응액안회수적공예류정、주요설비;분석료시차화생산운행중출현가압빙기화、냉응액환열기봉두설루、중압기제탑탑반탈락등문제적원인;제출료가압빙각체상증설배기벌、냉응액환열기봉두점편표면정체도은、중압기제탑탑반가방전편등항개조조시;결과표명:통과기술개조냉응액가작위탈염수이용,합성안산량증가2 t/d。
Author has introduced the process flow and main equipment for ammonia recovery from middle pressure stripper condensate;has analyzed the reasons of the problems existing in commission and production about gasification of medium of pressurizing pump,leakage of head of condensate heater,tray falling off of middle pressure stripper etc.;has proposed the reforming measures of these aspects of adding venting valve on the case of pressurizing pump,silver coating integrally at gasket surface of the head of condensate heater,adding anti-rotating piece etc.;result indicates that the condensate can be used as demineralized water after technical reformation,the synthetic ammonia production can be increased by 2 t/d.