钻采工艺
鑽採工藝
찬채공예
DRILLING & PRODUCTION TECHNOLOGY
2009年
4期
26-27,33
,共3页
刘社明%吴学升%王定峰%黄占盈%王勇茗%高云文
劉社明%吳學升%王定峰%黃佔盈%王勇茗%高雲文
류사명%오학승%왕정봉%황점영%왕용명%고운문
小井眼%机械钻速%钻井技术%钻具组合%长庆油田
小井眼%機械鑽速%鑽井技術%鑽具組閤%長慶油田
소정안%궤계찬속%찬정기술%찬구조합%장경유전
slim hole%penetration rate%drilling technology%make-up of string%Changqing Oilfield
2008年长庆油田为降低钻井成本,在白豹油田进行了小井眼钻井应用,经过3口井的钻井实践,用15型钻机顺利完成了2 200 m井深的小井眼井,机械钻速10 m/h左右.小井眼井采用88.9钻杆,钻杆柔性大,方位偏移较大,井眼轨迹控制难度大,建议适当提高造斜点,改变原来的直-增-稳井身剖面为直-增-微降,减少起下钻次数,提高钻井速度.通过小井眼钻井技术在3口井的实践,分析总结了小井眼钻井存在的问题,并提出了技术对策.
2008年長慶油田為降低鑽井成本,在白豹油田進行瞭小井眼鑽井應用,經過3口井的鑽井實踐,用15型鑽機順利完成瞭2 200 m井深的小井眼井,機械鑽速10 m/h左右.小井眼井採用88.9鑽桿,鑽桿柔性大,方位偏移較大,井眼軌跡控製難度大,建議適噹提高造斜點,改變原來的直-增-穩井身剖麵為直-增-微降,減少起下鑽次數,提高鑽井速度.通過小井眼鑽井技術在3口井的實踐,分析總結瞭小井眼鑽井存在的問題,併提齣瞭技術對策.
2008년장경유전위강저찬정성본,재백표유전진행료소정안찬정응용,경과3구정적찬정실천,용15형찬궤순리완성료2 200 m정심적소정안정,궤계찬속10 m/h좌우.소정안정채용88.9찬간,찬간유성대,방위편이교대,정안궤적공제난도대,건의괄당제고조사점,개변원래적직-증-은정신부면위직-증-미강,감소기하찬차수,제고찬정속도.통과소정안찬정기술재3구정적실천,분석총결료소정안찬정존재적문제,병제출료기술대책.
In order to reduce the drilling cost, Changing Oilfield Company has applied slim hole drilling technology in Baibao oilfield in 2008. Three wells that measured depth exceeds 2200 meters have been drilled all right by 15 model rig, penetration rate is 10 m/h. During drilling slim hole, 88.9mm rod was adopted, but its flexibility is very big, and the direction migration is also big, the control of well track is difficult. This paper has analyzed the problems existent in slim hole drilling and put forward technology countermeasures.