燃气涡轮试验与研究
燃氣渦輪試驗與研究
연기와륜시험여연구
GAS TURBINE EXPERIMENT AND RESEARCH
2012年
1期
54-57
,共4页
钱兴良%罗载奇%蒲晓霞%马前容
錢興良%囉載奇%蒲曉霞%馬前容
전흥량%라재기%포효하%마전용
直流起动发电机%输出轴%断裂%电源特性%冲击扭矩
直流起動髮電機%輸齣軸%斷裂%電源特性%遲擊扭矩
직류기동발전궤%수출축%단렬%전원특성%충격뉴구
direct current start generator%output shaft%rupture%power supply characteristic%impact torque
简述了某航空直流起动发电机输出轴在设计上为保护发动机安全而采取的措施,分析了引起直流起动发电机输出轴薄弱环节断裂的因素,确定了某小型发动机用起动发电机输出轴断裂的原因。根据该故障原因,制定了解决方案,并付诸试验验证。验证结果表明:排查分析得到的导致电机轴薄弱环节断裂的原因正确,制订的解决措施合理,效果令人满意。
簡述瞭某航空直流起動髮電機輸齣軸在設計上為保護髮動機安全而採取的措施,分析瞭引起直流起動髮電機輸齣軸薄弱環節斷裂的因素,確定瞭某小型髮動機用起動髮電機輸齣軸斷裂的原因。根據該故障原因,製定瞭解決方案,併付諸試驗驗證。驗證結果錶明:排查分析得到的導緻電機軸薄弱環節斷裂的原因正確,製訂的解決措施閤理,效果令人滿意。
간술료모항공직류기동발전궤수출축재설계상위보호발동궤안전이채취적조시,분석료인기직류기동발전궤수출축박약배절단렬적인소,학정료모소형발동궤용기동발전궤수출축단렬적원인。근거해고장원인,제정료해결방안,병부제시험험증。험증결과표명:배사분석득도적도치전궤축박약배절단렬적원인정학,제정적해결조시합리,효과령인만의。
The measures taken by the output shaft of an aviation direct current start generator are paper in- troduced for protecting the safety of the engine. And then the rupture factors of the output shaft weakness part are analyzed. Resolution was figured out according to the failure reason and was put to the experimenta- tion. The experimental results indicated that the analysis of output shaft rupture cause was correct, the reso- lution was reasonable and the effect was satisfying.