南水北调与水利科技
南水北調與水利科技
남수북조여수리과기
SOUTH-TO-NORTH WATER
2009年
6期
186-190,219
,共6页
段文刚%王才欢%黄国兵%韩黎明
段文剛%王纔歡%黃國兵%韓黎明
단문강%왕재환%황국병%한려명
水力学%流量系数%节制闸%原型观测%调水工程
水力學%流量繫數%節製閘%原型觀測%調水工程
수역학%류량계수%절제갑%원형관측%조수공정
hydraulics%discharge coefficient%check gates%prototype observation%water diversion project
京石段应急供水工程2008年临时通水系初次通水运行,总干渠输水控制和运行调度的水力学问题,一直为设计和运行管理等各方所关注.介绍6座典型节制闸流量系数原型观测成果,并进行水力计算分析评价.观测条件下,各节制闸出流均为闸孔淹没出流,其流量系数μ_1,介于0.773~0.834之间,平均为0.815.各闸过闸流昔实测值与计算值总体趋于一致,二者偏差介于-1%~5%之间,表明原型观测成果较为可靠,可为总干渠运行调度和输水控制提供技术支撑.
京石段應急供水工程2008年臨時通水繫初次通水運行,總榦渠輸水控製和運行調度的水力學問題,一直為設計和運行管理等各方所關註.介紹6座典型節製閘流量繫數原型觀測成果,併進行水力計算分析評價.觀測條件下,各節製閘齣流均為閘孔淹沒齣流,其流量繫數μ_1,介于0.773~0.834之間,平均為0.815.各閘過閘流昔實測值與計算值總體趨于一緻,二者偏差介于-1%~5%之間,錶明原型觀測成果較為可靠,可為總榦渠運行調度和輸水控製提供技術支撐.
경석단응급공수공정2008년림시통수계초차통수운행,총간거수수공제화운행조도적수역학문제,일직위설계화운행관리등각방소관주.개소6좌전형절제갑류량계수원형관측성과,병진행수력계산분석평개.관측조건하,각절제갑출류균위갑공엄몰출류,기류량계수μ_1,개우0.773~0.834지간,평균위0.815.각갑과갑류석실측치여계산치총체추우일치,이자편차개우-1%~5%지간,표명원형관측성과교위가고,가위총간거운행조도화수수공제제공기술지탱.
The hydraulics problems of water transfer control and operation dispatch in main channel of Jingshi Section are always draught attention of the designer and manager from the first time water transferring in 2008. It introduces the discharge coefficient prototype observation results of 6 check gates, hydraulic analysis is also included. Flow over check gates are all submergence sluice flow on observation conditions and the discharge coefficient μ_1 is about 0.773~0.834,in the average value of 0.815. Value of prototype observation of flow discharge over check gates is similar to computed value and the deviation is about -1%~5%. It is revealed that prototype observation results are reliable and the results can be a basis for water transfer dispatch of main channel