水电自动化与大坝监测
水電自動化與大壩鑑測
수전자동화여대패감측
HYDROPOWER AUTOMATION AND DAM MORNITORING
2011年
6期
55-58,77
,共5页
曲传勇%卢新民%高矿%王炜%罗帆%尚旭东
麯傳勇%盧新民%高礦%王煒%囉帆%尚旭東
곡전용%로신민%고광%왕위%라범%상욱동
黏土心墙坝%渗流监测%沉降监测
黏土心牆壩%滲流鑑測%沉降鑑測
점토심장패%삼류감측%침강감측
clay core dam%seepage monitoring%subsidence monitoring
通过对坝体0+090桩号及0+145桩号施工期沉降及渗流监测成果的分析,初步分析了铜场水库大坝施工期在孔隙压力水和上游水位的共同作用下,心墙内渗透水位上升和沉降量明显偏大的原因。监测成果表明:①坝体施工期沉降量偏大但沉降监测成果符合一般变化规律;②心墙碾压铺料层厚度较厚,层间结合部压实密度较低,心墙压实度较低的部位有少量水渗入;③0+090与0+145断面的倾度为0.001%~0.067%,说明心墙沉降比较均匀。
通過對壩體0+090樁號及0+145樁號施工期沉降及滲流鑑測成果的分析,初步分析瞭銅場水庫大壩施工期在孔隙壓力水和上遊水位的共同作用下,心牆內滲透水位上升和沉降量明顯偏大的原因。鑑測成果錶明:①壩體施工期沉降量偏大但沉降鑑測成果符閤一般變化規律;②心牆碾壓鋪料層厚度較厚,層間結閤部壓實密度較低,心牆壓實度較低的部位有少量水滲入;③0+090與0+145斷麵的傾度為0.001%~0.067%,說明心牆沉降比較均勻。
통과대패체0+090장호급0+145장호시공기침강급삼류감측성과적분석,초보분석료동장수고대패시공기재공극압력수화상유수위적공동작용하,심장내삼투수위상승화침강량명현편대적원인。감측성과표명:①패체시공기침강량편대단침강감측성과부합일반변화규률;②심장년압포료층후도교후,층간결합부압실밀도교저,심장압실도교저적부위유소량수삼입;③0+090여0+145단면적경도위0.001%~0.067%,설명심장침강비교균균。
The dam seepage monitoring is the monitoring and settlement of the clay core wall dam safety monitoring of important projects.Based on the dam and 0 +145 0 +090 Stake Stake construction period settlement and seepage monitoring results of the analysis,the initial prompt the dam construction period copper field in the pore water pressure and water level upstream of the joint action of the heart wall water level rise and subsidence within the penetration obviously too large causes.Monitoring results showed that: ① the settlement amount is too large dam construction period but the settlement monitoring results are consistent with the general variation;② heart wall thickness of compacted material spread thick layer with low density of the Ministry of compaction,degree of compaction than the core wall lower parts of a small amount of water infiltration;③ 0 +090 and 0 +145 section of the inclination of 0001% ~ 0067%,indicating more uniform core wall deposition.