天然气工业
天然氣工業
천연기공업
NATURAL GASINDUSTRY
2000年
4期
61-62
,共2页
李玉冠%张兴林%王新裕%康姬英%杜春
李玉冠%張興林%王新裕%康姬英%杜春
리옥관%장흥림%왕신유%강희영%두춘
柯克亚凝析气田%开采方式%反凝析%采收率%地层压力%开发效果
柯剋亞凝析氣田%開採方式%反凝析%採收率%地層壓力%開髮效果
가극아응석기전%개채방식%반응석%채수솔%지층압력%개발효과
Kekeya condensate field%Recovery method%Retrograde condensation%Recovery factor%Formation pressure%Development effectiveness
新疆柯克亚凝析气田经历勘探初期3口喷井的破坏和其后十年的衰竭式开采,地层压力大幅下降,地下反凝析现象严重,大量滞留在地层中的凝析油无法采出,开发效果差。1994年9月实施的西五一(3)气层组循环注气先导试验,有效地遏制了凝析气中重质组分在地下的反凝析,并通过注气过程中适时进行采气量、注采比和井网三方面的调整,使得凝析油采出程度较衰竭式开采方式的21%提高到37.9%,开发效果显著。
新疆柯剋亞凝析氣田經歷勘探初期3口噴井的破壞和其後十年的衰竭式開採,地層壓力大幅下降,地下反凝析現象嚴重,大量滯留在地層中的凝析油無法採齣,開髮效果差。1994年9月實施的西五一(3)氣層組循環註氣先導試驗,有效地遏製瞭凝析氣中重質組分在地下的反凝析,併通過註氣過程中適時進行採氣量、註採比和井網三方麵的調整,使得凝析油採齣程度較衰竭式開採方式的21%提高到37.9%,開髮效果顯著。
신강가극아응석기전경력감탐초기3구분정적파배화기후십년적쇠갈식개채,지층압력대폭하강,지하반응석현상엄중,대량체류재지층중적응석유무법채출,개발효과차。1994년9월실시적서오일(3)기층조순배주기선도시험,유효지알제료응석기중중질조분재지하적반응석,병통과주기과정중괄시진행채기량、주채비화정망삼방면적조정,사득응석유채출정도교쇠갈식개채방식적21%제고도37.9%,개발효과현저。
Beacause the Kekeya condensate gas field in Xinjiang Province suffered a blowout destruction of three wells in the initial stage of exploration and the successive natural de pletion production for ten years, its formation pressure was greatly declined and underground retrcgrade condensation was serious, which made a large number of condensate be detained in reservoir,so that its development effectiveness was bad. Carried out in September 1994, a precursory test of circulating gas injection in C51(3)gas reservoir effectively contained the underground
retrograde condensation of heavy components in condensate gas. Through timely adjusting the gas production, injection-produc tion ratio and well pattern in gas injection process, the recovery percent of condensate was raised from 21% in natural depletion production to 37.9 %, so that its development effectiveness was good.