环境科学学报
環境科學學報
배경과학학보
ACTA SCIENTIAE CIRCUMSTANTIAE
2001年
2期
134-139
,共6页
王琳%王宝贞%张维佳%王黛%杜显武%杨玉南%孔庆瑾
王琳%王寶貞%張維佳%王黛%杜顯武%楊玉南%孔慶瑾
왕림%왕보정%장유가%왕대%두현무%양옥남%공경근
铁%锰%有机微污染%臭氧化%活性炭%深度净化
鐵%錳%有機微汙染%臭氧化%活性炭%深度淨化
철%맹%유궤미오염%취양화%활성탄%심도정화
对铁、锰含量较高又存在有机微污染的原水进行深度处理的生产规模的净水厂(规模10m3/h),进行了运行效能的试验研究.该水厂由射流曝气→砂滤罐→臭氧接触氧化罐→生物活性炭滤罐→木鱼石滤罐→紫外线照射清水箱等处理单元组成.通过曝气充氧-砂滤预处理,去除溶解性的二价铁60%以上,在剩余臭氧的量为0.4mg/L(相应的臭氧投量为:4mg/L)的条件下,经臭氧接触氧化和生物活性炭过滤,在HRT 20min时,可去除铁锰高达100%,CODMn的去除率达90%左右.
對鐵、錳含量較高又存在有機微汙染的原水進行深度處理的生產規模的淨水廠(規模10m3/h),進行瞭運行效能的試驗研究.該水廠由射流曝氣→砂濾罐→臭氧接觸氧化罐→生物活性炭濾罐→木魚石濾罐→紫外線照射清水箱等處理單元組成.通過曝氣充氧-砂濾預處理,去除溶解性的二價鐵60%以上,在剩餘臭氧的量為0.4mg/L(相應的臭氧投量為:4mg/L)的條件下,經臭氧接觸氧化和生物活性炭過濾,在HRT 20min時,可去除鐵錳高達100%,CODMn的去除率達90%左右.
대철、맹함량교고우존재유궤미오염적원수진행심도처리적생산규모적정수엄(규모10m3/h),진행료운행효능적시험연구.해수엄유사류폭기→사려관→취양접촉양화관→생물활성탄려관→목어석려관→자외선조사청수상등처리단원조성.통과폭기충양-사려예처리,거제용해성적이개철60%이상,재잉여취양적량위0.4mg/L(상응적취양투량위:4mg/L)적조건하,경취양접촉양화화생물활성탄과려,재HRT 20min시,가거제철맹고체100%,CODMn적거제솔체90%좌우.
The experimental studies were carried out in a full scale advanced drinking water treatment plant treating raw water with higher concentrations of iron, manganese and organic matter with a capacity of 10m3/h, which has the following flow chart: aeration with an ejector→Sand fillter→Ozone contact column→BAC filter→Muyushi/sand filter→Clean water storage tank with UV radiation →Water distribution system. It was indicated from the experiment that the divalent soluble iron(Fe2+) was removed in the aeration-sand filtration stage by 60% or more; At the residual O3 content of 0.4mg/L from ozone contact column, corresponding ozone dosage of 4mg/L, the residual iron, manganese and organic matter was removed effectively in the ozone column and biological activated carbon filter through various mechanisms with removal efficiencies for iron, manganese and CODMn of 100%, 100% and some 90% respectively.