桂林工学院学报
桂林工學院學報
계림공학원학보
JOURNAL OF GUILIN INSTITUTE OF TECHNOLOGY
2009年
2期
262-265
,共4页
李晓良%王庆魁%王学立%吕中锋%季岭
李曉良%王慶魁%王學立%呂中鋒%季嶺
리효량%왕경괴%왕학립%려중봉%계령
低渗透油藏%开发效果%小井距%连通程度%压裂改造
低滲透油藏%開髮效果%小井距%連通程度%壓裂改造
저삼투유장%개발효과%소정거%련통정도%압렬개조
low permeability oil reservoir%recoverable reserve%infilling well spacing%connectivity degree%fracturing
舍女寺油田孔二段油藏空气渗透率26.7×10-3 μm2,开发过程中存在储层物性差、注水困难、注采井网不完善、油藏低速低效开采等问题.为此,开展了孔二段低渗油藏改善开发效果的4项研究,即提高水驱控制程度、合理驱动压力梯度、小井距加密提高连通程度和非主流线井压裂.实施后舍女寺油田孔二段油藏采油速度从0.81%上升到0.92%,最终采收率从14.8%提高到26.1%,增加可采储量38×104 t,为同类型油藏提供了改善开发效果的技术对策.
捨女寺油田孔二段油藏空氣滲透率26.7×10-3 μm2,開髮過程中存在儲層物性差、註水睏難、註採井網不完善、油藏低速低效開採等問題.為此,開展瞭孔二段低滲油藏改善開髮效果的4項研究,即提高水驅控製程度、閤理驅動壓力梯度、小井距加密提高連通程度和非主流線井壓裂.實施後捨女寺油田孔二段油藏採油速度從0.81%上升到0.92%,最終採收率從14.8%提高到26.1%,增加可採儲量38×104 t,為同類型油藏提供瞭改善開髮效果的技術對策.
사녀사유전공이단유장공기삼투솔26.7×10-3 μm2,개발과정중존재저층물성차、주수곤난、주채정망불완선、유장저속저효개채등문제.위차,개전료공이단저삼유장개선개발효과적4항연구,즉제고수구공제정도、합리구동압력제도、소정거가밀제고련통정도화비주류선정압렬.실시후사녀사유전공이단유장채유속도종0.81%상승도0.92%,최종채수솔종14.8%제고도26.1%,증가가채저량38×104 t,위동류형유장제공료개선개발효과적기술대책.
In the low permeability reservoir,there exist higher pressure in water injecting,poor injecting and discovery well-pattern,low speed and low effective in the development of Member 2 of Kongdian Formation in Shenvsi Oilfield.In order to solve these problems,four suggestions are proposed to improve the development in the low permeability oil reservoir, such as improving the degree of water flooding, optimizing technique of the reasonable driving pressure gradient, infilling well spacing and increasing the interconnected scale, reservoir fracturing for wells in the non-mainstream.After testing,the recovery rate enhances from 0.81% to 0.92%,and eventually recovery efficiency will be 14.8% to 26.18%,the increasing recoverable reserve will be 38×104 t.It provides a series of methods in improving similar reservoirs with low permeability.