大坝与安全
大壩與安全
대패여안전
LARGE DAM & SAFETY
2009年
2期
22-26
,共5页
克孜尔水库%防洪%安全
剋孜爾水庫%防洪%安全
극자이수고%방홍%안전
Kezier reservoir%flood control%safety
克孜尔水库由于初步设计中实测洪水资料系列较短,资料代表性不足,本次设计洪水复核在1984年补充初步设计的基础上,增加了1983~2006年的连续洪水系列.经复核,水库现状防洪能力达不到1000年一遇设计洪水标准,应采取工程措施使水库防洪能力达到设计要求.
剋孜爾水庫由于初步設計中實測洪水資料繫列較短,資料代錶性不足,本次設計洪水複覈在1984年補充初步設計的基礎上,增加瞭1983~2006年的連續洪水繫列.經複覈,水庫現狀防洪能力達不到1000年一遇設計洪水標準,應採取工程措施使水庫防洪能力達到設計要求.
극자이수고유우초보설계중실측홍수자료계렬교단,자료대표성불족,본차설계홍수복핵재1984년보충초보설계적기출상,증가료1983~2006년적련속홍수계렬.경복핵,수고현상방홍능력체불도1000년일우설계홍수표준,응채취공정조시사수고방홍능력체도설계요구.
Because of the lack of measured floods data series in preliminary design in 1984, analysis on flood control capacity of Kezier reservoir this time added the series of consecutive floods from 1983~2006. After review, it was found that the status of flood ontrol capacity of the reservoir was less than the design flood standard (1/1000). Engineering measures should be taken to im-prove flood control capacity. At the same time, the reservoir was located on sediment-laden river that its siltation was serious.With longer running time, flood control capacity of reservoir would be reduced. It was recommended that further study of reservoir siltation reduction measures should be carried out.