新疆石油地质
新疆石油地質
신강석유지질
XINJIANG PETROLEUM GEOLOGY
2009年
6期
725-727
,共3页
覃建华%丁艺%阳旭%池建萍%潘前樱%路培毅%林革
覃建華%丁藝%暘旭%池建萍%潘前櫻%路培毅%林革
담건화%정예%양욱%지건평%반전앵%로배의%림혁
克拉玛依油田%砾岩油藏%特低渗透油藏%小井距试验%加密井%开发层系
剋拉瑪依油田%礫巖油藏%特低滲透油藏%小井距試驗%加密井%開髮層繫
극랍마의유전%력암유장%특저삼투유장%소정거시험%가밀정%개발층계
Karamay field%conglomerate reservoir%low permeability%close spacing test%infill well%layer series of development
克拉玛依油田八区下乌尔禾组油藏为巨厚的特低渗透砾岩油藏,前期采用275 m井距反九点井网注水开发,油井见效低、压力保持程度低、采油速度低,低渗透储集层较大注采井距难以建立有效水驱是开发效果差的主要原因.小井距试验通过细分开发层系、缩小井距、改变井网方式以建立有效水驱体系.将开发层系细分为3套,逐层上返,首先试验P_2W_4,由275 m×388 m反九点井网加密为138 m×195 m反九点井网,后期转为五点井网平行裂缝方向注水.同时,控制单井注水量,采用点弱面强的注采政策.试验3 a后,与八区正常井距区块相比,各项开发指标明显好转,预计可提高采收率8.5%.
剋拉瑪依油田八區下烏爾禾組油藏為巨厚的特低滲透礫巖油藏,前期採用275 m井距反九點井網註水開髮,油井見效低、壓力保持程度低、採油速度低,低滲透儲集層較大註採井距難以建立有效水驅是開髮效果差的主要原因.小井距試驗通過細分開髮層繫、縮小井距、改變井網方式以建立有效水驅體繫.將開髮層繫細分為3套,逐層上返,首先試驗P_2W_4,由275 m×388 m反九點井網加密為138 m×195 m反九點井網,後期轉為五點井網平行裂縫方嚮註水.同時,控製單井註水量,採用點弱麵彊的註採政策.試驗3 a後,與八區正常井距區塊相比,各項開髮指標明顯好轉,預計可提高採收率8.5%.
극랍마의유전팔구하오이화조유장위거후적특저삼투력암유장,전기채용275 m정거반구점정망주수개발,유정견효저、압력보지정도저、채유속도저,저삼투저집층교대주채정거난이건립유효수구시개발효과차적주요원인.소정거시험통과세분개발층계、축소정거、개변정망방식이건립유효수구체계.장개발층계세분위3투,축층상반,수선시험P_2W_4,유275 m×388 m반구점정망가밀위138 m×195 m반구점정망,후기전위오점정망평행렬봉방향주수.동시,공제단정주수량,채용점약면강적주채정책.시험3 a후,여팔구정상정거구괴상비,각항개발지표명현호전,예계가제고채수솔8.5%.
Lower Wuerhe reservoir of District No.8 in Karamay oil field is a thick massive ultra-low permeability conglomerate reservoir,and was developed by waterflooding process with inverted nine-spot pattern and well spacing of 275 m in one series of strata in early stage.But it featured such poor development effects as the low efficiency of response for producers,low pressure maintenance degree and low oil production rate.The low permeability reservoir and larger producer-injector well spacing should be the main reasons for it was hard to establish effective waterflood response.This paper presents the close spacing pilot test that is to establish effective waterflood system by subdividing the layer series of development,decreasing the well spacing and changing the well patterns.The layer series of development is subdivided into three layers and recompleted layer by layer.The WU-4 unit is the first layer to be tested.The inverted nine-spot well pattern is infilled from 275 m×388 m to 138 m×195 m in the first stage and then converted into five-spot pattern to take a waterflood along parallel fractures,while controlling the injection flow rate by strategy of water drive weak at the spot and intensive in the area.Three-year test has shown that the production indices are all better than the original ones before,and it is expected that the recovery factor will be increased by 8.5%by this test.