襄樊学院学报
襄樊學院學報
양번학원학보
JOURNAL OF XIANGFAN UNIVERSITY
2011年
11期
29-34
,共6页
吴伟%殷泉东%吴国斌%胡熙平%申君健%郝恒泽%朱军
吳偉%慇泉東%吳國斌%鬍熙平%申君健%郝恆澤%硃軍
오위%은천동%오국빈%호희평%신군건%학항택%주군
套窜出砂井%油井治理技术%东辛油田
套竄齣砂井%油井治理技術%東辛油田
투찬출사정%유정치리기술%동신유전
Sand-drained well with casing channeling%Governing technology for oil well%Dongxin Oil Field
针对东辛油田部分套窜井出砂导致油井停产,影响单井开发效果的矛盾,应用套窜出砂井治理技术进行治理.2008年10月6日至2011年3月31日应用该技术共治理东辛油田不同区块的套窜出砂井4口,施工成功率100%,有效率100%.截止目前,正常生产下的4口井,恢复日产能24.3m3,平均日增油6.4m3,累计产油8 598.3m3,增油2 871.8m3,有效期最长的已超过937d且继续有效.该技术的成功应用为东辛油田同类井的治理提供了借鉴经验,并且具有货源广、成本低、适用范围广、有效期较长的特点.
針對東辛油田部分套竄井齣砂導緻油井停產,影響單井開髮效果的矛盾,應用套竄齣砂井治理技術進行治理.2008年10月6日至2011年3月31日應用該技術共治理東辛油田不同區塊的套竄齣砂井4口,施工成功率100%,有效率100%.截止目前,正常生產下的4口井,恢複日產能24.3m3,平均日增油6.4m3,纍計產油8 598.3m3,增油2 871.8m3,有效期最長的已超過937d且繼續有效.該技術的成功應用為東辛油田同類井的治理提供瞭藉鑒經驗,併且具有貨源廣、成本低、適用範圍廣、有效期較長的特點.
침대동신유전부분투찬정출사도치유정정산,영향단정개발효과적모순,응용투찬출사정치리기술진행치리.2008년10월6일지2011년3월31일응용해기술공치리동신유전불동구괴적투찬출사정4구,시공성공솔100%,유효솔100%.절지목전,정상생산하적4구정,회복일산능24.3m3,평균일증유6.4m3,루계산유8 598.3m3,증유2 871.8m3,유효기최장적이초과937d차계속유효.해기술적성공응용위동신유전동류정적치리제공료차감경험,병차구유화원엄、성본저、괄용범위엄、유효기교장적특점.
Owing to production halts resulting from some sand-drained well with casing channeling,a corresponding technology is presented.From October 6,2008 to March 31,2011,4 sand-drained wells with casing channeling are governed via this technology,both the success rate and the effective rate are 100%.So far,the daily capacity is 24.3m3,daily oil-increased is 6.4 m3,the accumulative total oil is 8598.3 m3 and the total oil-increased is 2871.8 m3.The longest effective period have exceeded 937 days and even continued to be effective.The technology is characteristic of rich supply of goods,low cost,broad scope of application and long period of validity.It is worth using for references for similar wells.