推进技术
推進技術
추진기술
JOURNAL OF PROPULSION TECHNOLOGY
2001年
2期
137-138,146
,共3页
张发启%江勇%桑增产%孔卫东
張髮啟%江勇%桑增產%孔衛東
장발계%강용%상증산%공위동
进气道%进气道-发动机匹配%进气道畸变%进气道试验%台架试验
進氣道%進氣道-髮動機匹配%進氣道畸變%進氣道試驗%檯架試驗
진기도%진기도-발동궤필배%진기도기변%진기도시험%태가시험
对某双转子涡喷发动机装与不装飞机进气道进行了台架对比实验,测量了发动机的状态参数和进口压力场。根据实验结果,分析了飞机进气道引起发动机的进气畸变和对发动机台架性能及台架点的影响,并讨论了造成变化的原因。实验结果对于正确使用该类型双转子涡喷发动机具有重要的现实意义。
對某雙轉子渦噴髮動機裝與不裝飛機進氣道進行瞭檯架對比實驗,測量瞭髮動機的狀態參數和進口壓力場。根據實驗結果,分析瞭飛機進氣道引起髮動機的進氣畸變和對髮動機檯架性能及檯架點的影響,併討論瞭造成變化的原因。實驗結果對于正確使用該類型雙轉子渦噴髮動機具有重要的現實意義。
대모쌍전자와분발동궤장여불장비궤진기도진행료태가대비실험,측량료발동궤적상태삼수화진구압력장。근거실험결과,분석료비궤진기도인기발동궤적진기기변화대발동궤태가성능급태가점적영향,병토론료조성변화적원인。실험결과대우정학사용해류형쌍전자와분발동궤구유중요적현실의의。
In the experimental research, a twin-rotor turbojet with aircraft's inlet was contrasted with the case without aircraft's inlet, and the state parameter and inlet's pressure field of the engine were measured. Based on the experimental result, the inlet distortion caused by aircraft's inlet, the effect of aircraft's inlet on the performance and platform point of the engine was analyzed as well as the relevant causes. The experimental result has practical significance for correctly using the twin-rotor turbojet.