采矿与安全工程学报
採礦與安全工程學報
채광여안전공정학보
JOURNAL OF MINING AND SAFETY ENGINEERING
2013年
3期
456-462
,共7页
卢平%方良才%童云飞%李贵和%章根发%邓中
盧平%方良纔%童雲飛%李貴和%章根髮%鄧中
로평%방량재%동운비%리귀화%장근발%산중
深井%煤层群%Y型通风%采空区%卸压瓦斯%抽采
深井%煤層群%Y型通風%採空區%卸壓瓦斯%抽採
심정%매층군%Y형통풍%채공구%사압와사%추채
deep mine%multipul coal seams%Y-type ventilation%gob%relieved gas%gas drainage
以朱集煤矿1111(1)工作面为例,针对深井高瓦斯低透气性煤层群首采层开采卸压瓦斯治理难题,将Y型通风工作面采空区瓦斯运移规律与采空区内部空隙储存卸压瓦斯的优势相结合,提出并实施了强化留巷墙体封闭和Y型通风工作面留巷段采空区卸压瓦斯抽采技术,结合地面钻井抽采采动上部卸压煤层瓦斯,实现了深井煤层群首采层工作面的安全高效回采。1111(1)工作面回采期间,绝对瓦斯涌出量最大72.39 m3/min,平均为43.64 m3/min,在工作面风量2290~2700 m3/min条件下,回风流瓦斯体积分数0.6%以下,平均瓦斯抽采量34.27 m3/min,其中埋管抽采瓦斯纯量平均为21.94 m3/min,占瓦斯抽采总量的64%,工作面回采期间瓦斯平均抽采率为78%,研究成果为今后类似深井煤层群首采层开采的卸压瓦斯抽采和治理提供技术指导。
以硃集煤礦1111(1)工作麵為例,針對深井高瓦斯低透氣性煤層群首採層開採卸壓瓦斯治理難題,將Y型通風工作麵採空區瓦斯運移規律與採空區內部空隙儲存卸壓瓦斯的優勢相結閤,提齣併實施瞭彊化留巷牆體封閉和Y型通風工作麵留巷段採空區卸壓瓦斯抽採技術,結閤地麵鑽井抽採採動上部卸壓煤層瓦斯,實現瞭深井煤層群首採層工作麵的安全高效迴採。1111(1)工作麵迴採期間,絕對瓦斯湧齣量最大72.39 m3/min,平均為43.64 m3/min,在工作麵風量2290~2700 m3/min條件下,迴風流瓦斯體積分數0.6%以下,平均瓦斯抽採量34.27 m3/min,其中埋管抽採瓦斯純量平均為21.94 m3/min,佔瓦斯抽採總量的64%,工作麵迴採期間瓦斯平均抽採率為78%,研究成果為今後類似深井煤層群首採層開採的卸壓瓦斯抽採和治理提供技術指導。
이주집매광1111(1)공작면위례,침대심정고와사저투기성매층군수채층개채사압와사치리난제,장Y형통풍공작면채공구와사운이규률여채공구내부공극저존사압와사적우세상결합,제출병실시료강화류항장체봉폐화Y형통풍공작면류항단채공구사압와사추채기술,결합지면찬정추채채동상부사압매층와사,실현료심정매층군수채층공작면적안전고효회채。1111(1)공작면회채기간,절대와사용출량최대72.39 m3/min,평균위43.64 m3/min,재공작면풍량2290~2700 m3/min조건하,회풍류와사체적분수0.6%이하,평균와사추채량34.27 m3/min,기중매관추채와사순량평균위21.94 m3/min,점와사추채총량적64%,공작면회채기간와사평균추채솔위78%,연구성과위금후유사심정매층군수채층개채적사압와사추채화치리제공기술지도。
In this paper, in view of the difficulties of relieved gas control in the first coal seam mining of the deep multiseams with high gas and low permeability, taking Coal Face 1111(1) in Zhuji Coal Mine as example, we provided and implemented the technique to strengthen the wall closeness of gob remained entry, and the gob relieved gas drainage technique in the gob remained entry of Y-type ventila-tion coal face, with the combination of gob gas delivery law in Y-type coal face and the advantage of accumulated relieved gas withtin the gob. In addition, combined with the gas drainage in the upper re-lieved coal seam by the surface well drilling, the safety and high efficiency mining in the first coal seamin of deep multiseams was realized. The results show that the maximal and average absolute gas emission quantity is 72.39 m3/min and 43.64 m3/min, respectively. When the air volume in the face is 2 290~2 700 m3/min, and the gas concentration in the return airflow is less than 0.6%, the average gas drainage volume is 34.27 m3/min, where the average gas drainage volume in buried pipes is about 21.94 m3/min, which is 64%of the total gas drainage volume. Moreover, the average gas drainage rate is about 78%during the mining process. The research achievement can provide the basis for gas drainage and control in the first coal seam mining of similar deep multiseams in the future.