混凝土
混凝土
혼응토
CONCRETE
2014年
8期
17-20
,共4页
李军涛%徐金俊%陈宗平%谭秋虹
李軍濤%徐金俊%陳宗平%譚鞦虹
리군도%서금준%진종평%담추홍
方钢管再生混凝土%中长柱%取代率%耗能%延性%刚度
方鋼管再生混凝土%中長柱%取代率%耗能%延性%剛度
방강관재생혼응토%중장주%취대솔%모능%연성%강도
recycled aggregate concrete filled square steel tube%medium long column%replacement ratio%energy dissipation%ductility%stiffness
为了揭示方钢管再生混凝土中长柱在轴心荷载作用下的性能退化规律,以再生粗骨料取代率和长细比为变化参数,完成了5个试件的轴心受压试验。在此基础上,分析了其延性指标、能量耗散、刚度退化的演化过程。研究结果表明:方钢管混凝土试件的峰值荷载比方钢管再生混凝土试件的大;随着再生粗骨料取代率的增加,方钢管再生混凝土轴压中长柱的耗能能力具有先降后升的趋势;方钢管混凝土试件的延性系数均比其再生混凝土试件的大;试件的弹性轴压刚度随取代率的增加表现为先增后减;随着长细比的增加,钢管再生混凝土中长柱的轴压耗能和弹性轴压刚度具有稳步减小的趋势,延性系数则呈现为先降低后增长之势。所得刚度退化的简化计算模型可为工程设计提供参考。
為瞭揭示方鋼管再生混凝土中長柱在軸心荷載作用下的性能退化規律,以再生粗骨料取代率和長細比為變化參數,完成瞭5箇試件的軸心受壓試驗。在此基礎上,分析瞭其延性指標、能量耗散、剛度退化的縯化過程。研究結果錶明:方鋼管混凝土試件的峰值荷載比方鋼管再生混凝土試件的大;隨著再生粗骨料取代率的增加,方鋼管再生混凝土軸壓中長柱的耗能能力具有先降後升的趨勢;方鋼管混凝土試件的延性繫數均比其再生混凝土試件的大;試件的彈性軸壓剛度隨取代率的增加錶現為先增後減;隨著長細比的增加,鋼管再生混凝土中長柱的軸壓耗能和彈性軸壓剛度具有穩步減小的趨勢,延性繫數則呈現為先降低後增長之勢。所得剛度退化的簡化計算模型可為工程設計提供參攷。
위료게시방강관재생혼응토중장주재축심하재작용하적성능퇴화규률,이재생조골료취대솔화장세비위변화삼수,완성료5개시건적축심수압시험。재차기출상,분석료기연성지표、능량모산、강도퇴화적연화과정。연구결과표명:방강관혼응토시건적봉치하재비방강관재생혼응토시건적대;수착재생조골료취대솔적증가,방강관재생혼응토축압중장주적모능능력구유선강후승적추세;방강관혼응토시건적연성계수균비기재생혼응토시건적대;시건적탄성축압강도수취대솔적증가표현위선증후감;수착장세비적증가,강관재생혼응토중장주적축압모능화탄성축압강도구유은보감소적추세,연성계수칙정현위선강저후증장지세。소득강도퇴화적간화계산모형가위공정설계제공삼고。
In order to reveal the degenerate rule of the mechanical behavior under the axial pressure of square steel tube reinforced recy-cled concrete intermediate length columns,5 specimens were axial-compression tested with the varied parameters of recycled coarse aggre-gate replacement ratio and slenderness ratio.On this basis,the evolutionary process of ductility index,energy dissipation and rigidity degen-eration were conducted research.As conclusion,the peak loads of square steel tube concrete columns were heavier than the recycled con-crete ones.The energy dissipation of recycled concrete columns went up after dropping along with the increase of replacement ratio.The ductility indexes of concrete columns were larger than the recycled ones.Elastic shaft rigidity dropped after going up along with the in-crease of replacement ratio.Energy dissipation of axial compression and elastic shaft rigidity declined steadily along with the increase of re-placement ratio,while the ductility index went up after dropping.The conclusive simplified model of rigidity degeneration could be served as a conference in practical engineering.