当代化工
噹代化工
당대화공
CONTEMPORARY CHEMICAL INDUSTRY
2014年
3期
327-329
,共3页
程秀玲%蒋林时%杨姣英%张玉霞%姜妍
程秀玲%蔣林時%楊姣英%張玉霞%薑妍
정수령%장림시%양교영%장옥하%강연
石化废水%MBBR%填充率
石化廢水%MBBR%填充率
석화폐수%MBBR%전충솔
Petrochemical wastewater%MBBR%Filling rate
实验主要研究填料填充率、水力停留时间、耐负荷冲击能力和通气量等因素对移动床生物膜反应器处理石化废水效果的影响。实验结果表明当填充率为30%,进水COD为362.06 mg/L、NH3-N为18.55 mg/L,停留时间为8 h时,COD去除率为90.2%;氨氮去除率达到80.5%;当通气量1.25 L/min,HRT为5 h时,COD的去除率能够达到86%;当进水有机负荷在0.9 kg COD/(m3·d)左右时, COD的去除率达到88%,此时出水COD小于40 mg/L。
實驗主要研究填料填充率、水力停留時間、耐負荷遲擊能力和通氣量等因素對移動床生物膜反應器處理石化廢水效果的影響。實驗結果錶明噹填充率為30%,進水COD為362.06 mg/L、NH3-N為18.55 mg/L,停留時間為8 h時,COD去除率為90.2%;氨氮去除率達到80.5%;噹通氣量1.25 L/min,HRT為5 h時,COD的去除率能夠達到86%;噹進水有機負荷在0.9 kg COD/(m3·d)左右時, COD的去除率達到88%,此時齣水COD小于40 mg/L。
실험주요연구전료전충솔、수력정류시간、내부하충격능력화통기량등인소대이동상생물막반응기처리석화폐수효과적영향。실험결과표명당전충솔위30%,진수COD위362.06 mg/L、NH3-N위18.55 mg/L,정류시간위8 h시,COD거제솔위90.2%;안담거제솔체도80.5%;당통기량1.25 L/min,HRT위5 h시,COD적거제솔능구체도86%;당진수유궤부하재0.9 kg COD/(m3·d)좌우시, COD적거제솔체도88%,차시출수COD소우40 mg/L。
The influence of filler filling rate, hydraulic retention time, resistance to shock loading capacity and ventilation and other factors on treatment effect of petrochemical wastewater by moving bed biofilm reactor was studied. The experimental results show that, when the stuffing rate is 30%, COD of influent is 362.06 mg/L, NH3-N is 18.55 mg/L,HTC is 8 h, COD removal efficiency can reach to 90.2%, removal rate of NH3-N can reach to 80.5%;When the ventilation is 1.25 L/min, HRT is 5 h, COD removal rate can reach to 86%;When the influent organic load is 0.9 kg COD/(m3 · d), COD removal efficiency can reach to 88%, and the effluent COD is less than 40 mg/L.