水利与建筑工程学报
水利與建築工程學報
수리여건축공정학보
TECHNIQUE OF SEEPAGE CONTROL
2013年
5期
1-4,9
,共5页
董玉莲%刘亚坤%孙洪亮%周乐
董玉蓮%劉亞坤%孫洪亮%週樂
동옥련%류아곤%손홍량%주악
消力坎%多级消能%弯曲溢洪道%模型试验%汤河水库
消力坎%多級消能%彎麯溢洪道%模型試驗%湯河水庫
소력감%다급소능%만곡일홍도%모형시험%탕하수고
baffle sill%multi-stage dissipation%curved spillway%model experiment%Tanghe Reservoir
弯曲溢洪道改扩建工程常需经过模型试验研究确定其消能优化方案,针对汤河水库除险加固工程改建方案中弯曲泄槽段急流冲击波及消能不充分等问题,通过水力学模型试验研究,推荐采用多级跌水与底流复合消能方式。在弯曲段一级消力池入口及出口设置斜向高低坎,二级消力池入口加消力坎、尾坎后设置防冲槽,形成多级跌水、两级消力池、消力坎、防冲槽等不同消能元件的组合,不仅有效利用了地形,而且改善了泄流流态,妥善解决了消能防冲问题。
彎麯溢洪道改擴建工程常需經過模型試驗研究確定其消能優化方案,針對湯河水庫除險加固工程改建方案中彎麯洩槽段急流遲擊波及消能不充分等問題,通過水力學模型試驗研究,推薦採用多級跌水與底流複閤消能方式。在彎麯段一級消力池入口及齣口設置斜嚮高低坎,二級消力池入口加消力坎、尾坎後設置防遲槽,形成多級跌水、兩級消力池、消力坎、防遲槽等不同消能元件的組閤,不僅有效利用瞭地形,而且改善瞭洩流流態,妥善解決瞭消能防遲問題。
만곡일홍도개확건공정상수경과모형시험연구학정기소능우화방안,침대탕하수고제험가고공정개건방안중만곡설조단급류충격파급소능불충분등문제,통과수역학모형시험연구,추천채용다급질수여저류복합소능방식。재만곡단일급소력지입구급출구설치사향고저감,이급소력지입구가소력감、미감후설치방충조,형성다급질수、량급소력지、소력감、방충조등불동소능원건적조합,불부유효이용료지형,이차개선료설류류태,타선해결료소능방충문제。
The model experiment is widely used as a key method to determine the reconstruction scheme of curved spill-way.With regard to the project problems as the torrent shock wave in curved chute and flood discharge energy dissipation in the reconstruction scheme of Tanghe Reservoir,a composite energy dissipation system of multi-stage plunge with bottom flow is recommended based on model-test results.The scheme is composed of the first-stage stilling basin with two high-low slope banks at the inlet and outlet in the curved chute and the second-stage stilling basin which has a baffle sill at the inlet and an anti-scour trench behind the baffle wall.The combination of various dissipators,including multi-stage plunge,two-stage stilling basin,baffle sill and anti-scour trench,could not only make full use of the terrain,but also improve the flow condition,thus properly solving the energy dissipation and scour prevention of the spillway.