振动与冲击
振動與遲擊
진동여충격
JOURNAL OF VIBRATION AND SHOCK
2014年
3期
117-121,144
,共6页
张俊红%王健%毕凤荣%刘海%李林洁%李忠鹏
張俊紅%王健%畢鳳榮%劉海%李林潔%李忠鵬
장준홍%왕건%필봉영%류해%리림길%리충붕
机体振动%经验模态分解%时频分析%结构优化
機體振動%經驗模態分解%時頻分析%結構優化
궤체진동%경험모태분해%시빈분석%결구우화
engine block vibration%empirical mode decomposition (EMD)%time-frequency analysis%structural op-timization
为降低柴油机机体振动,开展了基于经验模态分解(EMD)和时频分析的低振动机体优化设计研究。首先建立了机体有限元模型,通过机体模态试验验证了有限元模型正确性;然后,采用多体动力学和有限元相结合的方法计算了机体振动响应,并将计算结果与试验结果进行了对比验证,两者比较吻合;进而采用EMD对机体裙部振动速度信号进行分解,对分解得到的结果中能量较大的分量进行小波时频变换,通过时频分析得到结构优化的主要依据;最后对优化前后振动响应分别采用小波和 Hilbert 变换进行定性和定量的对比验证。结果表明,优化后整机振动烈度降低了26.81%,整机的振动水平得到了明显的降低,从而验证了该方法的有效性。
為降低柴油機機體振動,開展瞭基于經驗模態分解(EMD)和時頻分析的低振動機體優化設計研究。首先建立瞭機體有限元模型,通過機體模態試驗驗證瞭有限元模型正確性;然後,採用多體動力學和有限元相結閤的方法計算瞭機體振動響應,併將計算結果與試驗結果進行瞭對比驗證,兩者比較吻閤;進而採用EMD對機體裙部振動速度信號進行分解,對分解得到的結果中能量較大的分量進行小波時頻變換,通過時頻分析得到結構優化的主要依據;最後對優化前後振動響應分彆採用小波和 Hilbert 變換進行定性和定量的對比驗證。結果錶明,優化後整機振動烈度降低瞭26.81%,整機的振動水平得到瞭明顯的降低,從而驗證瞭該方法的有效性。
위강저시유궤궤체진동,개전료기우경험모태분해(EMD)화시빈분석적저진동궤체우화설계연구。수선건립료궤체유한원모형,통과궤체모태시험험증료유한원모형정학성;연후,채용다체동역학화유한원상결합적방법계산료궤체진동향응,병장계산결과여시험결과진행료대비험증,량자비교문합;진이채용EMD대궤체군부진동속도신호진행분해,대분해득도적결과중능량교대적분량진행소파시빈변환,통과시빈분석득도결구우화적주요의거;최후대우화전후진동향응분별채용소파화 Hilbert 변환진행정성화정량적대비험증。결과표명,우화후정궤진동열도강저료26.81%,정궤적진동수평득도료명현적강저,종이험증료해방법적유효성。
In order to reduce diesel engine block vibration,a low-vibration block optimization design was proposed based on empirical mode decomposition (EMD)and time-frequency analysis.Firstly,Multibody Dynamics and finite element method were used to simulate the engine block vibration and the simulation results were verified very well compared with the test results.Then,EMD was used to decompose the vibration velocity signal of crankcase skirt of an engine.And one component of the decomposed results having the largest vibration energy was transformed with wavelet time-frequency analysis.The time-frequency analysis results provided a main basis for structural optimization.At last,the vibration responses of the original block and those of the optimized structure were compared qualitatively with the wavelet analysis and quantitatively with Hilbert transformation,respectively.Results showed that the vibrating intensity of the optimized block decreases 26.81% and the engine vibration is dramaticlly reduced;therefore,the effectiveness of the proposed method is verified.