石油与天然气化工
石油與天然氣化工
석유여천연기화공
CHEMICAL ENGINEERING OF OIL AND GAS
2014年
1期
1-5
,共5页
张大秋%敬季昀%杨林%王棠昱
張大鞦%敬季昀%楊林%王棠昱
장대추%경계윤%양림%왕당욱
原油%硫化氢%H2S%气提脱硫%脱硫剂
原油%硫化氫%H2S%氣提脫硫%脫硫劑
원유%류화경%H2S%기제탈류%탈류제
crude oil%hydrogen sulfide%H2S%gas stripping%desulfurizer
针对我国西部某油田A井区高含硫的问题,利用专业软件模拟和相关实验开展了井场原油气提脱硫技术和化学脱硫技术的研究。在模拟A井气提脱硫的基础上,得出气提法的优化参数为塔压0.3MPa,6层塔板,气提气量和塔底重沸器温度依据气提气充足与否和耗能情况进行调节,气提气量控制在4.7~6.1 m3/t,相应的塔底重沸器温度为152.0~41.6℃。对于化学脱硫,通过实验筛选出了适用于A井、主要成分为二异丙基合成物的脱硫剂,并评价了用量、作用时间、含水率、温度等因素对其脱硫效果的影响。
針對我國西部某油田A井區高含硫的問題,利用專業軟件模擬和相關實驗開展瞭井場原油氣提脫硫技術和化學脫硫技術的研究。在模擬A井氣提脫硫的基礎上,得齣氣提法的優化參數為塔壓0.3MPa,6層塔闆,氣提氣量和塔底重沸器溫度依據氣提氣充足與否和耗能情況進行調節,氣提氣量控製在4.7~6.1 m3/t,相應的塔底重沸器溫度為152.0~41.6℃。對于化學脫硫,通過實驗篩選齣瞭適用于A井、主要成分為二異丙基閤成物的脫硫劑,併評價瞭用量、作用時間、含水率、溫度等因素對其脫硫效果的影響。
침대아국서부모유전A정구고함류적문제,이용전업연건모의화상관실험개전료정장원유기제탈류기술화화학탈류기술적연구。재모의A정기제탈류적기출상,득출기제법적우화삼수위탑압0.3MPa,6층탑판,기제기량화탑저중비기온도의거기제기충족여부화모능정황진행조절,기제기량공제재4.7~6.1 m3/t,상응적탑저중비기온도위152.0~41.6℃。대우화학탈류,통과실험사선출료괄용우A정、주요성분위이이병기합성물적탈류제,병평개료용량、작용시간、함수솔、온도등인소대기탈류효과적영향。
The existence of hydrogen sulfide in crude oil will cause the corrosion of the equip-ment ,lower oil quality and a serious threat to personal safety .Therefore ,it is important to re-move hydrogen sulfide in the process of crude oil production .To solve the problem of high-sulfur crude oil produced in A well area in the western China ,the gas stripping method and the chemical method have both been analyzed .Based on the stimulation of stripping process ,the optimized pa-rameters of gas stripping are obtained ,namely tower pressure is 0 .3 MPa ,plate number is 6 , stripping gas is 4 .7 -6 .1 m3/t ,and reboiler temperature is 152 .0 -41 .6 ℃ ,the amount of stripping gas and the reboiler temperature are adjusted according to the adequacy of gas and the energy consumption . The desulfurizer mainly composed of two isopropyl complexes has been screened out and the effect of dosage ,operating time ,water content ,temperature on the desulfu-rization have also been evaluated .