化工进展
化工進展
화공진전
CHEMICAL INDUSTRY AND ENGINEERING PROGRESS
2012年
11期
2574-2576,2585
,共4页
吴杰%王建红%赵显文%王生伟%林宏%瞿朝霞
吳傑%王建紅%趙顯文%王生偉%林宏%瞿朝霞
오걸%왕건홍%조현문%왕생위%림굉%구조하
裂解汽油%加氢催化剂%再生
裂解汽油%加氫催化劑%再生
렬해기유%가경최화제%재생
pyrolysis gasoline%hydrogenation catalyst%regeneration
2009年,LY-9802催化剂作为国内一家大型合资石油化工企业的新建裂解汽油加氢装置的首装剂投入使用。运行结果表明,该催化剂第一运行周期为31个月,在入口温度为225~241℃、压力为2.67 MPa、进料量为33~48 t/h的条件下,硫含量小于0.2 mg/kg,溴价小于0.1 gBr/100g;经过再生处理后,该催化剂已稳定运转3个月,在入口温度为248℃、压力为2.67 MPa、进料量为46 t/h的条件下,硫含量小于0.2 mg/kg,溴价小于0.1 gBr/100g。
2009年,LY-9802催化劑作為國內一傢大型閤資石油化工企業的新建裂解汽油加氫裝置的首裝劑投入使用。運行結果錶明,該催化劑第一運行週期為31箇月,在入口溫度為225~241℃、壓力為2.67 MPa、進料量為33~48 t/h的條件下,硫含量小于0.2 mg/kg,溴價小于0.1 gBr/100g;經過再生處理後,該催化劑已穩定運轉3箇月,在入口溫度為248℃、壓力為2.67 MPa、進料量為46 t/h的條件下,硫含量小于0.2 mg/kg,溴價小于0.1 gBr/100g。
2009년,LY-9802최화제작위국내일가대형합자석유화공기업적신건렬해기유가경장치적수장제투입사용。운행결과표명,해최화제제일운행주기위31개월,재입구온도위225~241℃、압력위2.67 MPa、진료량위33~48 t/h적조건하,류함량소우0.2 mg/kg,추개소우0.1 gBr/100g;경과재생처리후,해최화제이은정운전3개월,재입구온도위248℃、압력위2.67 MPa、진료량위46 t/h적조건하,류함량소우0.2 mg/kg,추개소우0.1 gBr/100g。
LY-9802 was applied in a newly built 2nd stage pyrolysis gasoline hydrogenation unit in a large-scale jointly invested petrochemical enterprise.Result showed that the first regeneration cycle was 31 months.Under the inlet temperature of 225-241℃,pressure of 2.67MPa,raw rate of 33-48 t/h,sulfur content of hydrogenation production is less than 0.2mg/kg,BrV is less than 0.1gBr/100g.After regeneration,the catalyst has run stably for 3 month so far.Under the inlet temperature of 248 ℃,pressure of 2.67MPa,raw rate of 46t/h,sulfur content of hydrogenation production is less than 0.2mg/kg,BrV is less than 0.1gBr/100g.