广州化工
廣州化工
엄주화공
GUANGZHOU CHEMICAL INDUSTRY AND TECHNOLOGY
2013年
24期
34-36
,共3页
方朝合%黄志龙%郑德温%葛稚新%李小龙
方朝閤%黃誌龍%鄭德溫%葛稚新%李小龍
방조합%황지룡%정덕온%갈치신%리소룡
油砂%水洗分离工艺%分离剂配方%试验
油砂%水洗分離工藝%分離劑配方%試驗
유사%수세분리공예%분리제배방%시험
oil sand%hot water extraction technology%extraction agent formula%tests
2006~2009年,中国石油勘探开发研究院廊坊分院在准噶尔盆地西北缘风城地区开展了油砂资源勘探和水洗分离工艺技术研究,落实该区油砂油可采资源量5498万t,平均含油率为7.1%~10%,分布于白垩系和侏罗系,厚度80~140 m,油砂顶层埋深在50~90 m,针对该区油砂特点开展了油砂水洗分离机理研究,成功研制了该区油砂水洗分离剂配方,该配方药剂浓度在4%,温度85℃的情况下,分离率达到了90%。在系列研究的基础上,完成了该区年处理1万t油砂的试验现场建设,开展油砂现场分离试验,常态运行收油率达90%,水洗工艺技术及装备研发取得成功。
2006~2009年,中國石油勘探開髮研究院廊坊分院在準噶爾盆地西北緣風城地區開展瞭油砂資源勘探和水洗分離工藝技術研究,落實該區油砂油可採資源量5498萬t,平均含油率為7.1%~10%,分佈于白堊繫和侏囉繫,厚度80~140 m,油砂頂層埋深在50~90 m,針對該區油砂特點開展瞭油砂水洗分離機理研究,成功研製瞭該區油砂水洗分離劑配方,該配方藥劑濃度在4%,溫度85℃的情況下,分離率達到瞭90%。在繫列研究的基礎上,完成瞭該區年處理1萬t油砂的試驗現場建設,開展油砂現場分離試驗,常態運行收油率達90%,水洗工藝技術及裝備研髮取得成功。
2006~2009년,중국석유감탐개발연구원랑방분원재준갈이분지서북연풍성지구개전료유사자원감탐화수세분리공예기술연구,락실해구유사유가채자원량5498만t,평균함유솔위7.1%~10%,분포우백성계화주라계,후도80~140 m,유사정층매심재50~90 m,침대해구유사특점개전료유사수세분리궤리연구,성공연제료해구유사수세분리제배방,해배방약제농도재4%,온도85℃적정황하,분리솔체도료90%。재계렬연구적기출상,완성료해구년처리1만t유사적시험현장건설,개전유사현장분리시험,상태운행수유솔체90%,수세공예기술급장비연발취득성공。
From 2007 to 2008, Research Institute of Petroleum Exploration & Development, Langfang Branch Launched oil sand resource exploration and the study of hot water extraction technology in Fengcheng area, Northwest of Junggar Basin, and the recoverable tar sand oil resource is 5498 million tons with the oil content in 7.1%~10%, which is distributed in Cretaceous and Jurassic with the thickness of 80 ~140 meters, the cover depth of oil sand is 50 ~90 meters.Combining with the characteristics of the oil sand in this area and based on the research of hot water extraction mechanism in oil sand, the hot water extraction agent formula for the oil sand in this area had been successfully developed, and its separation rate reached 90%, provided that the concentrations of the agent was 4%and the separation temperature was 85 ℃.Based on series of study, the construction of testing site, which was capable of processing 10000 tons oil sand in this area, was completed, and the on-site extraction tests of oil sand were launched with the recovery rate of 90% in normal operation, and the hot water extraction technology and equipment research & development were successful.