燃料与化工
燃料與化工
연료여화공
FUEL & CHEMICAL PROCESSES
2014年
2期
53-55,58
,共4页
真空碳酸钾%脱硫%改进
真空碳痠鉀%脫硫%改進
진공탄산갑%탈류%개진
Vacuum potassium carbonate%Desulfurization%Improvement
针对真空碳酸钾脱硫工艺在开工初期出现的问题,经过工艺改进和操作优化后,解决了真空泵堵塞、酸汽管道堵塞、再生效率不高、克劳斯炉频繁连锁、硫冷凝器堵塞等问题,降低了KOH溶液消耗,提高了脱硫效率,脱硫塔后煤气中H2 S含量降至250mg/m3以下,生产稳定正常。
針對真空碳痠鉀脫硫工藝在開工初期齣現的問題,經過工藝改進和操作優化後,解決瞭真空泵堵塞、痠汽管道堵塞、再生效率不高、剋勞斯爐頻繁連鎖、硫冷凝器堵塞等問題,降低瞭KOH溶液消耗,提高瞭脫硫效率,脫硫塔後煤氣中H2 S含量降至250mg/m3以下,生產穩定正常。
침대진공탄산갑탈류공예재개공초기출현적문제,경과공예개진화조작우화후,해결료진공빙도새、산기관도도새、재생효솔불고、극로사로빈번련쇄、류냉응기도새등문제,강저료KOH용액소모,제고료탈류효솔,탈류탑후매기중H2 S함량강지250mg/m3이하,생산은정정상。
At the beginning of start up,the desulfurization process by vacuum potassium carbonate method has some problems.After taking relevant measures in process and operation ,the problems such as blockage of vacuum pump ,blockage of acid gas pipe,low regeneration efficiency,frequent in-terlock of Claus furnace and blockage of sulfur condenser are solved .Desulfurization efficiency is increased with low KOH solution consumption.H2 S content in gas is reduced to less than 250mg/m 3 after desulfurization,and the system is running stably .