南水北调与水利科技
南水北調與水利科技
남수북조여수리과기
SOUTH-TO-NORTH WATER
2014年
2期
142-145
,共4页
马述江%乔裕民%黄志全%高文荣
馬述江%喬裕民%黃誌全%高文榮
마술강%교유민%황지전%고문영
南水北调%液化%标准贯入试验%跨孔波速试验
南水北調%液化%標準貫入試驗%跨孔波速試驗
남수북조%액화%표준관입시험%과공파속시험
South-to-North Water Diversion%liquefaction%standard penetration test%crosshole wave velocity test
南水北调中线总干渠磁县段的地基土具有中等震动液化现象,如处理不当可能导致渠道沉陷甚至滑坡,危及渠道安全。设计采用夯扩挤密碎石桩进行地基处理,为此需在现场选取有代表性的场地上进行试桩,通过试验验证不同桩间距对砂土液化的处理效果,以确定合适的桩间距,为大面积施工提供有关参数和依据。夯扩挤密碎石桩利用重锤冲击成孔,分层填入碎石或其他置换料,并夯击至设计标高。试验表明,采用桩间土标准贯入试验可判断经处理后的地基土,桩间距为1.8m时不存在液化,桩间距为1.9m时存在液化。原位跨孔剪切波速试验结果显示,处理后桩间土的剪切波速较地基处理前提高较多,证明挤密效果明显。
南水北調中線總榦渠磁縣段的地基土具有中等震動液化現象,如處理不噹可能導緻渠道沉陷甚至滑坡,危及渠道安全。設計採用夯擴擠密碎石樁進行地基處理,為此需在現場選取有代錶性的場地上進行試樁,通過試驗驗證不同樁間距對砂土液化的處理效果,以確定閤適的樁間距,為大麵積施工提供有關參數和依據。夯擴擠密碎石樁利用重錘遲擊成孔,分層填入碎石或其他置換料,併夯擊至設計標高。試驗錶明,採用樁間土標準貫入試驗可判斷經處理後的地基土,樁間距為1.8m時不存在液化,樁間距為1.9m時存在液化。原位跨孔剪切波速試驗結果顯示,處理後樁間土的剪切波速較地基處理前提高較多,證明擠密效果明顯。
남수북조중선총간거자현단적지기토구유중등진동액화현상,여처리불당가능도치거도침함심지활파,위급거도안전。설계채용항확제밀쇄석장진행지기처리,위차수재현장선취유대표성적장지상진행시장,통과시험험증불동장간거대사토액화적처리효과,이학정합괄적장간거,위대면적시공제공유관삼수화의거。항확제밀쇄석장이용중추충격성공,분층전입쇄석혹기타치환료,병항격지설계표고。시험표명,채용장간토표준관입시험가판단경처리후적지기토,장간거위1.8m시불존재액화,장간거위1.9m시존재액화。원위과공전절파속시험결과현시,처리후장간토적전절파속교지기처리전제고교다,증명제밀효과명현。
Foundation soil of Ci-Xian section of the main canal in the Middle Route of South-to-North Water Transfer Project has medium liquefaction phenomenon .Canal subsidence and landslide can happen if the foundation soil is not treated properly ,which can affect canal safety .The ram-compaction gravel piles can decrease sand ground liquefaction .In-situ pile test needs to be con-ducted .The effects of different pile spacing on treatment of sand liquefaction were tested to determine the appropriate pile spac-ing ,which can support the design parameters and principle for pile construction in a large area .The ram-compaction gravel piles used heavy hammer impact to form the hole ,and then filled in gravel or other replacement materials in each layer to reach the design height .The results showed that ground liquefaction is not shown when the pile spacing is 1 .8 m but occurs when the pile spacing is 1 .9 m .In addition ,the shear wave test of original crosshole showed that the shear wave velocity of soil among piles increases after the treatment ,which indicated the compaction effect is significant .