人民黄河
人民黃河
인민황하
Yellow River
2014年
3期
117-119,122
,共4页
段鸿锋%邓军%刘超%刘小江
段鴻鋒%鄧軍%劉超%劉小江
단홍봉%산군%류초%류소강
消能防冲%优化%阶梯溢洪道%扭曲挑坎%真金万水库
消能防遲%優化%階梯溢洪道%扭麯挑坎%真金萬水庫
소능방충%우화%계제일홍도%뉴곡도감%진금만수고
energy dissipation%optimize%stepped spillway%skew bucket%Zhenjinwan Reservoir
针对真金万水库溢洪道出口水流流速快、冲刷右岸边坡的问题,通过水工模型试验研究,取消了原设计方案中阶梯溢洪道下游消力池,而在溢洪道末端增设扭曲挑坎,并对扭曲坎进行优化,提出了利用两边直线段加中间小圆弧斜切挑坎的扭曲坎体形,获得了较好的水舌分散效果和入流流态。推荐方案的试验结果表明:阶梯+扭曲挑坎联合消能方案能够很好地解决真金万水库溢洪道的消能防冲问题,且阶梯和扭曲坎自身结构安全满足工程要求。
針對真金萬水庫溢洪道齣口水流流速快、遲刷右岸邊坡的問題,通過水工模型試驗研究,取消瞭原設計方案中階梯溢洪道下遊消力池,而在溢洪道末耑增設扭麯挑坎,併對扭麯坎進行優化,提齣瞭利用兩邊直線段加中間小圓弧斜切挑坎的扭麯坎體形,穫得瞭較好的水舌分散效果和入流流態。推薦方案的試驗結果錶明:階梯+扭麯挑坎聯閤消能方案能夠很好地解決真金萬水庫溢洪道的消能防遲問題,且階梯和扭麯坎自身結構安全滿足工程要求。
침대진금만수고일홍도출구수류류속쾌、충쇄우안변파적문제,통과수공모형시험연구,취소료원설계방안중계제일홍도하유소력지,이재일홍도말단증설뉴곡도감,병대뉴곡감진행우화,제출료이용량변직선단가중간소원호사절도감적뉴곡감체형,획득료교호적수설분산효과화입류류태。추천방안적시험결과표명:계제+뉴곡도감연합소능방안능구흔호지해결진금만수고일홍도적소능방충문제,차계제화뉴곡감자신결구안전만족공정요구。
Aiming at settling the issue of high velocity of Zhenjinwan Reservoir spillway outlet and the scour of the right side slope of downstream river caused by the plunging flow,we abolished the stilling pool downstream of the spillway and instead set a skew bucket which was chamfered with straight lines on the two sides and a small arc in the middle was increased at the end of the spillway based on hydro-model test. Our test on the rec-ommendation scheme shows that the"steps and skew bucket" joint energy dissipation is a good solution to the Zhenjinwan Reservoir spillway energy dissipation and erosion problems,at the same time both the steps and the skew bucket are safety in structure.