吉林水利
吉林水利
길림수리
JI LIN WATER RESOURCES
2014年
3期
31-35
,共5页
刘中峰%邱静%黄本胜%王丽雯
劉中峰%邱靜%黃本勝%王麗雯
류중봉%구정%황본성%왕려문
白石窑%水位下降%断面模型%面流消能%流态
白石窯%水位下降%斷麵模型%麵流消能%流態
백석요%수위하강%단면모형%면류소능%류태
Baishyao%drawdown%sectional model%surface flow energy dissipation%flow state
针对白石窑水利枢纽下游水位降低可能影响水闸泄洪消能的问题,分下游河床下切前、后两种情况,选取典型工况进行了断面模型试验研究。试验表明,枢纽下游水位降低基本不会改变水闸下泄水流原有消能流态,下泄水流的主要消能条件变化不明显。但局开控泄、电站甩负荷工况及流量低于500m3/s时,下游水位下降导致下游河床流速增加且水深较小,可能对河床造成冲刷,建议适当增加开启孔数,减小下泄单宽流量,确保泄洪安全。
針對白石窯水利樞紐下遊水位降低可能影響水閘洩洪消能的問題,分下遊河床下切前、後兩種情況,選取典型工況進行瞭斷麵模型試驗研究。試驗錶明,樞紐下遊水位降低基本不會改變水閘下洩水流原有消能流態,下洩水流的主要消能條件變化不明顯。但跼開控洩、電站甩負荷工況及流量低于500m3/s時,下遊水位下降導緻下遊河床流速增加且水深較小,可能對河床造成遲刷,建議適噹增加開啟孔數,減小下洩單寬流量,確保洩洪安全。
침대백석요수리추뉴하유수위강저가능영향수갑설홍소능적문제,분하유하상하절전、후량충정황,선취전형공황진행료단면모형시험연구。시험표명,추뉴하유수위강저기본불회개변수갑하설수류원유소능류태,하설수류적주요소능조건변화불명현。단국개공설、전참솔부하공황급류량저우500m3/s시,하유수위하강도치하유하상류속증가차수심교소,가능대하상조성충쇄,건의괄당증가개계공수,감소하설단관류량,학보설홍안전。
The typical section of the river are chosen and carried on model test research based on downstream river before cut and after cut,for Baishiyao Water Control downstream water level reducing maybe impact sluice gate energy dissipation;Tests showed that lowering of water level downstream does not change the origi-nal discharge flow energy dissipation of sluice ,the main energy dissipation conditions of downstream flow changed obviously.But partly discharge flow,power load shedding and flow conditions below the 500m3/s,the downstream water level decline resulting in downstream river flow rate increases and the water depth is small , it may cause erosion of the riverbed,recommend appropriate to increase the number of open gates,reducing discharged single wide flow,ensure flood safety.