电镀与涂饰
電鍍與塗飾
전도여도식
ELECTROPLATING & FINISHING
2014年
10期
425-428
,共4页
马桂君%王长军%曼得拉·查汗%易桂虎%王伊诺
馬桂君%王長軍%曼得拉·查汗%易桂虎%王伊諾
마계군%왕장군%만득랍·사한%역계호%왕이낙
导管架%乙二醇%储罐%防腐%热喷铝%涂层缺陷
導管架%乙二醇%儲罐%防腐%熱噴鋁%塗層缺陷
도관가%을이순%저관%방부%열분려%도층결함
jacket%monoethylene glycol%storage tank%corrosion protection%thermal sprayed aluminum%coating defect
讨论了 LW3-1导管架腿贫乙二醇(MEG)储罐热喷铝工艺表面处理要求和影响热喷铝质量的因素,总结了施工过程中出现的质量问题,包括焊缝处起皮、环板涂层脱落、附着力未达要求等,提出了相应的解决方案:增加环板焊缝打磨和内部缺陷打磨工艺,以消除钝化层和表面缺陷的影响;采用16#氧化铝喷砂增大表面粗糙度;采用大功率通风机减少施工过程中粉尘的影响;改变喷涂方式,加强设备检查和工人培训等。通过采取以上措施,有效地提高了热喷铝的质量。MEG罐热喷铝涂层厚度在180~300μm之间,附着力单点测试值在7 MPa以上,平均值在9 MPa以上。
討論瞭 LW3-1導管架腿貧乙二醇(MEG)儲罐熱噴鋁工藝錶麵處理要求和影響熱噴鋁質量的因素,總結瞭施工過程中齣現的質量問題,包括銲縫處起皮、環闆塗層脫落、附著力未達要求等,提齣瞭相應的解決方案:增加環闆銲縫打磨和內部缺陷打磨工藝,以消除鈍化層和錶麵缺陷的影響;採用16#氧化鋁噴砂增大錶麵粗糙度;採用大功率通風機減少施工過程中粉塵的影響;改變噴塗方式,加彊設備檢查和工人培訓等。通過採取以上措施,有效地提高瞭熱噴鋁的質量。MEG罐熱噴鋁塗層厚度在180~300μm之間,附著力單點測試值在7 MPa以上,平均值在9 MPa以上。
토론료 LW3-1도관가퇴빈을이순(MEG)저관열분려공예표면처리요구화영향열분려질량적인소,총결료시공과정중출현적질량문제,포괄한봉처기피、배판도층탈락、부착력미체요구등,제출료상응적해결방안:증가배판한봉타마화내부결함타마공예,이소제둔화층화표면결함적영향;채용16#양화려분사증대표면조조도;채용대공솔통풍궤감소시공과정중분진적영향;개변분도방식,가강설비검사화공인배훈등。통과채취이상조시,유효지제고료열분려적질량。MEG관열분려도층후도재180~300μm지간,부착력단점측시치재7 MPa이상,평균치재9 MPa이상。
The requirement of surface treatment of thermal spraying aluminum process for lean glycol (MEG) storage tank in LW3-1 jacket legs and the factors influencing the quality of thermal sprayed aluminum were discussed. The quality problems existing in construction were summarized, including the peeling in weld bead, flaking-off of coating on annular plate, and poor adhesion. Some corresponding resolutions were presented: polishing the weld beads on annular plate and internal defects to eliminate the effect of passivation film and surface defect; sand blasting with No.16 alumina to increase the surface roughness;applying a high-power ventilator to decrease the effect of dust during construction;changing the spraying method;and enhancing the inspection of equipments and the training of workers. The thermal sprayed aluminum coating on MEG storage tank had a thickness ranging from 180 μm to 300 μm. The adhesion strength of the coating was higher than 7 MPa at single spot and 9 MPa averagely, indicating that the quality of thermal spayed aluminum was improved effectively.