水利水电科技进展
水利水電科技進展
수이수전과기진전
ADVANCES IN SCIENCE AND TECHNOLOGY OF WATER RESOURCES
2014年
2期
11-15
,共5页
郎韵%臧英平%唐洪武%曾诚%王玲玲%肖洋
郎韻%臧英平%唐洪武%曾誠%王玲玲%肖洋
랑운%장영평%당홍무%증성%왕령령%초양
三汊河河口闸%导流墙%泄流特性%整流措施%秦淮河%长江
三汊河河口閘%導流牆%洩流特性%整流措施%秦淮河%長江
삼차하하구갑%도류장%설류특성%정류조시%진회하%장강
Sanchahe River Gate%guide wall%discharge characteristics%flow regulation measures%Qinhuai River%Yangtze River
针对外秦淮河入江口的三汊河河口闸大流量泄洪时过闸水流不均的问题,建立了江河水闸大范围水深平均二维数学模型来研究河口闸的泄流特性,并利用河工模型试验结果率定模型参数。对长江不同水位流量组合及河口闸上游河床地形修整工况下河口闸大流量泄流特性模拟计算结果表明,导致过闸水流不均的主要因素是河势及河道深泓位置;河口闸上游阻水建筑物的拆除对过闸偏流的改善作用有限;37 m墙长结合5毅偏角的导流墙可有效改善过闸水流不均的现状。
針對外秦淮河入江口的三汊河河口閘大流量洩洪時過閘水流不均的問題,建立瞭江河水閘大範圍水深平均二維數學模型來研究河口閘的洩流特性,併利用河工模型試驗結果率定模型參數。對長江不同水位流量組閤及河口閘上遊河床地形脩整工況下河口閘大流量洩流特性模擬計算結果錶明,導緻過閘水流不均的主要因素是河勢及河道深泓位置;河口閘上遊阻水建築物的拆除對過閘偏流的改善作用有限;37 m牆長結閤5毅偏角的導流牆可有效改善過閘水流不均的現狀。
침대외진회하입강구적삼차하하구갑대류량설홍시과갑수류불균적문제,건립료강하수갑대범위수심평균이유수학모형래연구하구갑적설류특성,병이용하공모형시험결과솔정모형삼수。대장강불동수위류량조합급하구갑상유하상지형수정공황하하구갑대류량설류특성모의계산결과표명,도치과갑수류불균적주요인소시하세급하도심홍위치;하구갑상유조수건축물적탁제대과갑편류적개선작용유한;37 m장장결합5의편각적도류장가유효개선과갑수류불균적현상。
In order to deal with the deflection of flow passing through the Sanchahe River Gate, which is located at the conjunction of the external Qinhuai River and the Yangzte River, under large discharges, a two-dimensional depth-averaged mathematical model was developed to investigate the discharge characteristics. Experimental results from river models were used to calibrate the model parameters. Several typical operating conditions, including different combinations of the water level and the discharge of the Yangtze River and the correction of the upstream riverbed topography, were studied. The numerical simulation results show the following:the main reasons for the serious deflection of flow are the river regime and the location of the river thalweg; removing the water-blocking facilities upstream of the gate has limited influence in improving the pattern of flow passing through the gate;a guide wall with a length of 37 m and a deflection angle of 5o can improve the pattern of flow passing through the gate significantly.