路基工程
路基工程
로기공정
SUBGRADE ENGINEERING
2012年
2期
81-85
,共5页
动静力排水固结%加固深度%加固效果%淤泥质地基处理
動靜力排水固結%加固深度%加固效果%淤泥質地基處理
동정력배수고결%가고심도%가고효과%어니질지기처리
dynamic-static drainage consolidation%reinforced depth%reinforced effect%muck foundation disposal
结合广州南沙港淤泥地基处理工程,利用超孔隙水压力、分层沉降和抗剪强度等指标,对动静力排水固结法加固淤泥地基的加固深度和加固效果进行现场试验研究。结果表明,增加总夯击能可明显地增大有效加固深度;夯击能一定时,夯击四遍或五遍,每遍点夯的夯击能控制在900kN·m以下时,加固效果和加固深度均优于夯击三遍,重锤低落距夯击方式的加固深度和加固效果优于轻锤高落距。
結閤廣州南沙港淤泥地基處理工程,利用超孔隙水壓力、分層沉降和抗剪彊度等指標,對動靜力排水固結法加固淤泥地基的加固深度和加固效果進行現場試驗研究。結果錶明,增加總夯擊能可明顯地增大有效加固深度;夯擊能一定時,夯擊四遍或五遍,每遍點夯的夯擊能控製在900kN·m以下時,加固效果和加固深度均優于夯擊三遍,重錘低落距夯擊方式的加固深度和加固效果優于輕錘高落距。
결합엄주남사항어니지기처리공정,이용초공극수압력、분층침강화항전강도등지표,대동정력배수고결법가고어니지기적가고심도화가고효과진행현장시험연구。결과표명,증가총항격능가명현지증대유효가고심도;항격능일정시,항격사편혹오편,매편점항적항격능공제재900kN·m이하시,가고효과화가고심도균우우항격삼편,중추저락거항격방식적가고심도화가고효과우우경추고락거。
Combining with the project of muck foundation disposal at Nansha Port, Guangzhou and using the indexes, such as excess pore water pressure, layered settlement and shearing strength, the depth and the effect of the reinforcement on muck foundation by means of dynamic-static drainage consolidation are studied through on-site experiment. The result shows that the increment of total tamping energy can increase the effective reinforced depth obviously. When tamping energy is given, tamping four or five times with the tamping energy in single point every time to be controlled less than 900 kN. m has superior reinforced effect and depth than tamping three times ; the reinforced depth and effect by means of heavy hammer and low drop distance tamping are superior to those by light hammer and high drop distance.