当代化工
噹代化工
당대화공
CONTEMPORARY CHEMICAL INDUSTRY
2013年
12期
1765-1767
,共3页
焦化液化气%脱硫醇%降总硫
焦化液化氣%脫硫醇%降總硫
초화액화기%탈류순%강총류
Delayed coking LPG%Mercaptan removal unit%Total sulfur reduction
天津石化在炼制高硫原油时,焦化液化气胺脱后总硫高达16000 mg/Nm3,导致原焦化液化气脱硫醇装置的产品不合格,产品总硫在1000 mg/Nm3左右,在作为民用燃料销售时需要掺兑硫含量较低的催化液化气或降低价格,严重影响了天津石化的经济效益。为此,中石化炼油事业部组织 SEI、天津石化和河北精致有限公司进行了长达2年的攻关和优化改造,采用液化气深度脱硫专利技术,成功解决了焦化液化气硫形态复杂、脱除难的问题,脱硫后焦化液化气总硫降低到100 mg/Nm3以下,达到通过气体分馏装置生产合格丙烯的要求,成为中石化焦化液化气深度脱硫和利用的首个成功案例。
天津石化在煉製高硫原油時,焦化液化氣胺脫後總硫高達16000 mg/Nm3,導緻原焦化液化氣脫硫醇裝置的產品不閤格,產品總硫在1000 mg/Nm3左右,在作為民用燃料銷售時需要摻兌硫含量較低的催化液化氣或降低價格,嚴重影響瞭天津石化的經濟效益。為此,中石化煉油事業部組織 SEI、天津石化和河北精緻有限公司進行瞭長達2年的攻關和優化改造,採用液化氣深度脫硫專利技術,成功解決瞭焦化液化氣硫形態複雜、脫除難的問題,脫硫後焦化液化氣總硫降低到100 mg/Nm3以下,達到通過氣體分餾裝置生產閤格丙烯的要求,成為中石化焦化液化氣深度脫硫和利用的首箇成功案例。
천진석화재련제고류원유시,초화액화기알탈후총류고체16000 mg/Nm3,도치원초화액화기탈류순장치적산품불합격,산품총류재1000 mg/Nm3좌우,재작위민용연료소수시수요참태류함량교저적최화액화기혹강저개격,엄중영향료천진석화적경제효익。위차,중석화련유사업부조직 SEI、천진석화화하북정치유한공사진행료장체2년적공관화우화개조,채용액화기심도탈류전리기술,성공해결료초화액화기류형태복잡、탈제난적문제,탈류후초화액화기총류강저도100 mg/Nm3이하,체도통과기체분류장치생산합격병희적요구,성위중석화초화액화기심도탈류화이용적수개성공안례。
As Tianjin petrochemical Co., Ltd (TPCC) refines high-sulfur crude oil, total sulfur content of delayed coking LPG is up to 16 000 mg/Nm3 after amine treating,which can cause that the product of mercaptan removal unit is unqualified. When total sulfur content of product is around 1000 mg/Nm3,the product can be sold as domestic fuel by mixing the low-sulfur LPG or reducing its price, which will seriously affect economic benefits of TPCC. Therefore, Sinopec refining division organized SEI, TPCC and Hebei Jingzhi technology company to carry out technical research and optimizing reformation. By using the LPG deep desulfurization patented technology, the problem that sulfur in delayed coking LPG is hard to be removed has been successfully solved. The total sulfur after treatment is less than 100 mg/Nm3, which can be used to produce propylene though gas fractionation unit.