广东水利电力职业技术学院学报
廣東水利電力職業技術學院學報
엄동수리전력직업기술학원학보
JOURNAL OF GUANGDONG TECHNICAL COLLEGE OF WATER RESOURCES AND ELECTRIC ENGINEERING
2014年
1期
1-3
,共3页
黄智敏%钟勇明%陈卓英%付波
黃智敏%鐘勇明%陳卓英%付波
황지민%종용명%진탁영%부파
溢流坝%溢流堰%压强%优化%研究
溢流壩%溢流堰%壓彊%優化%研究
일류패%일류언%압강%우화%연구
overflow dam%overflow weir%pressure%optimization%research
乐昌峡水电站溢流坝属高水头、大流量泄水建筑物,溢流坝设置了5孔泄洪孔口,其溢流堰采用WES型曲线。水力模型试验表明,初设方案的溢流堰面出现了较大的负压值,不能满足设计规范的要求,堰面有可能会产生空蚀破坏。为此在分析溢流堰面产生负压原因的基础上,对溢流堰面体型进行修改和优化,结果明显降低了溢流堰面的负压值,有利于工程的安全运行。
樂昌峽水電站溢流壩屬高水頭、大流量洩水建築物,溢流壩設置瞭5孔洩洪孔口,其溢流堰採用WES型麯線。水力模型試驗錶明,初設方案的溢流堰麵齣現瞭較大的負壓值,不能滿足設計規範的要求,堰麵有可能會產生空蝕破壞。為此在分析溢流堰麵產生負壓原因的基礎上,對溢流堰麵體型進行脩改和優化,結果明顯降低瞭溢流堰麵的負壓值,有利于工程的安全運行。
악창협수전참일류패속고수두、대류량설수건축물,일류패설치료5공설홍공구,기일류언채용WES형곡선。수력모형시험표명,초설방안적일류언면출현료교대적부압치,불능만족설계규범적요구,언면유가능회산생공식파배。위차재분석일류언면산생부압원인적기출상,대일류언면체형진행수개화우화,결과명현강저료일류언면적부압치,유리우공정적안전운행。
The overflow dam of Lechangxia hydropower station is a high head and large flow sluice structure. The dam has set up 5 release flood orifice,and the overflow weir is used by WES curve. The hydraulic model test shows that the overflow weir surface of the preliminary design scheme appears larger negative pressure value. As the value can not meet the requirements of the design specification, the weir surface may cause cavitations damage. Based on the analysis of causes of the overflow weir surface negative pressure in this paper, the overflow weir surface shape is modified and optimized, and the pressure is significantly reduced which is conducive to the safe operation of the project.