浙江水利科技
浙江水利科技
절강수리과기
ZHEJIANG SHUILI KEJI
2012年
2期
5-9
,共5页
溢洪道%挑流消能%RNGκ-ε紊流模型%三维数值模拟
溢洪道%挑流消能%RNGκ-ε紊流模型%三維數值模擬
일홍도%도류소능%RNGκ-ε문류모형%삼유수치모의
spillway%trajectory energy dissipation%RNGκ-ε turbulent model%3D numerical simulation
采用FLOW-3D水流计算软件模拟了溢洪道挑流消能的三维水流流场,并通过调整溢洪道平面布置、增设贴角和改变预挖冲坑范围等措施对溢洪道原设计方案进行了优化。结合水工模型试验成果,对原设计方案和优化方案的水流流态、流速分布和水面线等水力特性进行了对比分析。数值模拟计算结果与水工模型试验比较吻合,说明优化方案的有效性,也进一步表明三维数值模拟的可行性。
採用FLOW-3D水流計算軟件模擬瞭溢洪道挑流消能的三維水流流場,併通過調整溢洪道平麵佈置、增設貼角和改變預挖遲坑範圍等措施對溢洪道原設計方案進行瞭優化。結閤水工模型試驗成果,對原設計方案和優化方案的水流流態、流速分佈和水麵線等水力特性進行瞭對比分析。數值模擬計算結果與水工模型試驗比較吻閤,說明優化方案的有效性,也進一步錶明三維數值模擬的可行性。
채용FLOW-3D수류계산연건모의료일홍도도류소능적삼유수류류장,병통과조정일홍도평면포치、증설첩각화개변예알충갱범위등조시대일홍도원설계방안진행료우화。결합수공모형시험성과,대원설계방안화우화방안적수류류태、류속분포화수면선등수력특성진행료대비분석。수치모의계산결과여수공모형시험비교문합,설명우화방안적유효성,야진일보표명삼유수치모의적가행성。
The three-dimensional flow field of spillway was numerically simulated using FLOW-3D software.The optimal solution include adjusting plane arrangement of spillway,pulsing bucket and changing pre-dug hole extent of the original spillway.Combining hydraulic model tests,flow pattern,velocity distribution,water surface profile and other hydraulic characteristics of the original program and optimal program flow were analyzed.The value of hydraulic model tests and numerical simulation calculations are in good agreement,which demonstrate the effectiveness of optimization,also shows the feasibility of three-dimensional numerical simulation.