动力工程学报
動力工程學報
동력공정학보
JOURNAL OF POWER ENGINEERING
2012年
4期
282-288
,共7页
何国安%闵昌发%张学延%张卫军%王延博
何國安%閔昌髮%張學延%張衛軍%王延博
하국안%민창발%장학연%장위군%왕연박
汽轮发电机组%600MW%轴系%振动%动平衡
汽輪髮電機組%600MW%軸繫%振動%動平衡
기륜발전궤조%600MW%축계%진동%동평형
turbo-generator set%600 MW%shaft system%vibration%dynamic balance
针对国产600MW汽轮发电机组运行中普遍存在的轴系异常振动问题,分析了振动现象、振动特征、振动机理及其原因,并对现场动平衡问题的处理方法进行了总结.结果表明:国产600MW高中压转子由于结构不对称存在较大的振型干扰,现场对转子进行动平衡时应考虑各阶振型的干扰系数,尤其是一阶配重对二阶振型的影响;部分机组低压转子轴承座振动超标的原因为采用坐缸式轴承座的支承刚度不足,现场可以通过精细动平衡来消除;发电机转子振动主要呈现三阶振型,现场校正三阶不平衡的方法就是在低-发对轮或发-励对轮上加重,且在动平衡分析时应注意区分振型畸变;集电小轴的振动受发-励对轮的安装工况影响较大,现场对其进行动平衡分析时应考虑发-励对轮下张口对加重响应的影响.
針對國產600MW汽輪髮電機組運行中普遍存在的軸繫異常振動問題,分析瞭振動現象、振動特徵、振動機理及其原因,併對現場動平衡問題的處理方法進行瞭總結.結果錶明:國產600MW高中壓轉子由于結構不對稱存在較大的振型榦擾,現場對轉子進行動平衡時應攷慮各階振型的榦擾繫數,尤其是一階配重對二階振型的影響;部分機組低壓轉子軸承座振動超標的原因為採用坐缸式軸承座的支承剛度不足,現場可以通過精細動平衡來消除;髮電機轉子振動主要呈現三階振型,現場校正三階不平衡的方法就是在低-髮對輪或髮-勵對輪上加重,且在動平衡分析時應註意區分振型畸變;集電小軸的振動受髮-勵對輪的安裝工況影響較大,現場對其進行動平衡分析時應攷慮髮-勵對輪下張口對加重響應的影響.
침대국산600MW기륜발전궤조운행중보편존재적축계이상진동문제,분석료진동현상、진동특정、진동궤리급기원인,병대현장동평형문제적처리방법진행료총결.결과표명:국산600MW고중압전자유우결구불대칭존재교대적진형간우,현장대전자진행동평형시응고필각계진형적간우계수,우기시일계배중대이계진형적영향;부분궤조저압전자축승좌진동초표적원인위채용좌항식축승좌적지승강도불족,현장가이통과정세동평형래소제;발전궤전자진동주요정현삼계진형,현장교정삼계불평형적방법취시재저-발대륜혹발-려대륜상가중,차재동평형분석시응주의구분진형기변;집전소축적진동수발-려대륜적안장공황영향교대,현장대기진행동평형분석시응고필발-려대륜하장구대가중향응적영향.
Aiming at the vibration problems frequently occurring in operation of domestic 600 MW turbo-generator sets,an analysis has been carried out on the vibration phenomenon,feature,mechanism and the causes,while various countermeasures for on-site dynamic balancing summarized.Results show that large vibration disturbance exists in domestic 600 MW high-and medium-pressure rotors due to their asymmetric structures,to overcome which,the disturbance coefficient of various vibration modes and orders should be considered during on-site dynamic balancing process of rotors,especially the influence of one-order weighing on two-order vibration mode.The abnormal vibration occurring in low-pressure cylinder of some domestic sets are caused by insufficient rigidity of supports for relevant bearing seats,which may be handled by fine dynamic balancing on site.The vibration of generator rotor is mainly of the three-order mode,which may be corrected by adding balancing weight on the shaft coupling between low-pressure rotor and generator rotor,or on the shaft coupling between generator rotor and exciter rotor,in consideration of the distortion of vibration mode.The vibration of electricity gathering shaft is highly affected by the installation quality of the shaft coupling between generator rotor and exciter rotor,for which attention should be paid to the influence of weighing response at bottom opening of the shaft coupling between generator rotor and exciter rotor,during corresponding dynamic balancing analysis on site.