广东化工
廣東化工
엄동화공
GUANGDONG CHEMICAL INDUSTRY
2012年
17期
41-42,52
,共3页
周年忠%田文广%顾宇昕%李雁%陶红秀%解新安
週年忠%田文廣%顧宇昕%李雁%陶紅秀%解新安
주년충%전문엄%고우흔%리안%도홍수%해신안
PRO%II%间歇反应精馏%模拟优化
PRO%II%間歇反應精餾%模擬優化
PRO%II%간헐반응정류%모의우화
PRO/II%batch reactive distillation%simulation and optimization
针对对苯二甲酸(PTA)和新戊二醇(NPG)合成聚对苯二甲酸戊二酯(PPT)出现的问题,应用PRO/II化工模拟软件对间歇反应精馏过程进行模拟优化,模拟结果与实际生产数据相吻合,相对误差在0.29%~7.85%之间;提出了减少塔顶馏出液中新戊二醇含量、精馏时间的工艺优化方案:以该工艺优化方案为依据对生产装置改造,改造后与改造前相比,精馏时间缩短了2.92h。
針對對苯二甲痠(PTA)和新戊二醇(NPG)閤成聚對苯二甲痠戊二酯(PPT)齣現的問題,應用PRO/II化工模擬軟件對間歇反應精餾過程進行模擬優化,模擬結果與實際生產數據相吻閤,相對誤差在0.29%~7.85%之間;提齣瞭減少塔頂餾齣液中新戊二醇含量、精餾時間的工藝優化方案:以該工藝優化方案為依據對生產裝置改造,改造後與改造前相比,精餾時間縮短瞭2.92h。
침대대분이갑산(PTA)화신무이순(NPG)합성취대분이갑산무이지(PPT)출현적문제,응용PRO/II화공모의연건대간헐반응정류과정진행모의우화,모의결과여실제생산수거상문합,상대오차재0.29%~7.85%지간;제출료감소탑정류출액중신무이순함량、정류시간적공예우화방안:이해공예우화방안위의거대생산장치개조,개조후여개조전상비,정류시간축단료2.92h。
Batch reactive distillation process was simulated by using the PRO/II software. The relative deviation of component content of NPG, water in tower top and distillation time were 4.02 %, 7.85 % and 0.29 % comparing with the production data respectively. The process optimization cases were proposed, compared with the original production data with the optimum proposal, distillation time could be shortened by 2.92 h.