石油与天然气化工
石油與天然氣化工
석유여천연기화공
CHEMICAL ENGINEERING OF OIL AND GAS
2013年
6期
582-587
,共6页
廖铁%苏梦瑶%李法璋%范秦
廖鐵%囌夢瑤%李法璋%範秦
료철%소몽요%리법장%범진
蒸汽%凝结水%优化%节能%硫磺回收
蒸汽%凝結水%優化%節能%硫磺迴收
증기%응결수%우화%절능%류광회수
steam%condensation water%optimization%energy saving%sulfur recovery
对万州天然气净化厂硫磺回收单元的蒸汽与凝结水构成进行了分析,并对蒸汽引射器重新选型以实现蒸汽梯级利用,以及采用凝结水罐排空蒸汽回收、凝结水循环利用、凝结水分压回收、蒸汽疏水阀优化选型以实现凝结水密闭式回收等优化措施作了详细的分析探讨。实施各项优化措施后,每处理1×104m3原料天然气(H2S质量分数为1%),综合能耗由1303.38MJ降为最低约1188.23MJ,与每处理1×104m3原料天然气(H2S质量分数为1%)综合能耗为2010MJ的设计值相比,节能效果明显。
對萬州天然氣淨化廠硫磺迴收單元的蒸汽與凝結水構成進行瞭分析,併對蒸汽引射器重新選型以實現蒸汽梯級利用,以及採用凝結水罐排空蒸汽迴收、凝結水循環利用、凝結水分壓迴收、蒸汽疏水閥優化選型以實現凝結水密閉式迴收等優化措施作瞭詳細的分析探討。實施各項優化措施後,每處理1×104m3原料天然氣(H2S質量分數為1%),綜閤能耗由1303.38MJ降為最低約1188.23MJ,與每處理1×104m3原料天然氣(H2S質量分數為1%)綜閤能耗為2010MJ的設計值相比,節能效果明顯。
대만주천연기정화엄류광회수단원적증기여응결수구성진행료분석,병대증기인사기중신선형이실현증기제급이용,이급채용응결수관배공증기회수、응결수순배이용、응결수분압회수、증기소수벌우화선형이실현응결수밀폐식회수등우화조시작료상세적분석탐토。실시각항우화조시후,매처리1×104m3원료천연기(H2S질량분수위1%),종합능모유1303.38MJ강위최저약1188.23MJ,여매처리1×104m3원료천연기(H2S질량분수위1%)종합능모위2010MJ적설계치상비,절능효과명현。
Based on the composition analysis of steam and condensation water of sulfur recov-ery unit in Wanzhou branch of Chongqing natural gas purification plant , this paper discussed these optimization measures . The steam ejector was redesigned to realize the application of stream cascading and the methods are used to realize the airtight recycling of condensation water such as recovering steam discharged from the condensation tank ,recycling condensation water ,re-covering condensation water at partial pressure and optimizing the type of steam traps .The com-prehensive energy consumption can be reduced from 1 303 .38 MJ to 1 188 .23 MJ per 1 × 104 m3 containing 1% (mol) of H2S after optimization .Compared with the design which consumes 2 010 MJ per 1 × 104 m3 containing 1% (mol) of H2 S ,the effect of energy saving is obvious .