自动化博览
自動化博覽
자동화박람
AUTOMAITON PANORAMA
2013年
z2期
110-115
,共6页
王正风%陈晓锋%罗亚桥%徐斌
王正風%陳曉鋒%囉亞橋%徐斌
왕정풍%진효봉%라아교%서빈
变电站%相位%电流波形%3次谐波%串联谐振%并联谐振
變電站%相位%電流波形%3次諧波%串聯諧振%併聯諧振
변전참%상위%전류파형%3차해파%천련해진%병련해진
Transformer Substation%Phasic%Current Wave%The Third Harmonic%Series Resonance%Parallel Resonance
针对220kV板桥变低压侧3组高压并联电容器装置(以下简称电容器装置)投运时,主变高压侧和低压侧三相电流出现相位和波形畸变进行分析。通过现场谐波检测,并进行系统仿真等值计算分析,发现其缘由是由于220kV系统中存在3次谐波电压源,且因板桥变低压侧电容器装置参数配置不合理,导致产生3次谐波串联谐振条件引起3次谐波电流放大,从而造成板桥变高压侧和低压侧电流相位和波形畸变。通过将板桥变其中1组电容器装置内5%串联电抗器调整为12%串联电抗器,以抑制3次谐波的放大,保证了板桥变的正常启动。
針對220kV闆橋變低壓側3組高壓併聯電容器裝置(以下簡稱電容器裝置)投運時,主變高壓側和低壓側三相電流齣現相位和波形畸變進行分析。通過現場諧波檢測,併進行繫統倣真等值計算分析,髮現其緣由是由于220kV繫統中存在3次諧波電壓源,且因闆橋變低壓側電容器裝置參數配置不閤理,導緻產生3次諧波串聯諧振條件引起3次諧波電流放大,從而造成闆橋變高壓側和低壓側電流相位和波形畸變。通過將闆橋變其中1組電容器裝置內5%串聯電抗器調整為12%串聯電抗器,以抑製3次諧波的放大,保證瞭闆橋變的正常啟動。
침대220kV판교변저압측3조고압병련전용기장치(이하간칭전용기장치)투운시,주변고압측화저압측삼상전류출현상위화파형기변진행분석。통과현장해파검측,병진행계통방진등치계산분석,발현기연유시유우220kV계통중존재3차해파전압원,차인판교변저압측전용기장치삼수배치불합리,도치산생3차해파천련해진조건인기3차해파전류방대,종이조성판교변고압측화저압측전류상위화파형기변。통과장판교변기중1조전용기장치내5%천련전항기조정위12%천련전항기,이억제3차해파적방대,보증료판교변적정상계동。
Both high voltage side and low side of transformer current phasic and wave have been badly changed when the 3 sets of capacitors start up in 220kV transformer substation of Banqiao. . Based on scene test date analysis and system simulation compute, the reason has been found. The voltage resource of third harmonic in 220kV power system and irrational parameter of capacitors is proposed. Irrational parameter of capacitors result in series resonance, so the third harmonic blow up. Both the current phasic and wave have badly changed. The third harmonic blowup can be restrained by reactance ratio adjustment form 5% to 12%in one set of capacitor. So, 220kV transformer substation of Banqiao can be normal put into operation.