安徽理工大学学报(自然科学版)
安徽理工大學學報(自然科學版)
안휘리공대학학보(자연과학판)
JOURNAL OF ANHUI UNIVERSITY OF SCIENCE AND TECHNOLOGY(NATURAL SCIENCE)
2014年
2期
79-82
,共4页
张义俊%余大有%夏红兵%张雷%郑应键
張義俊%餘大有%夏紅兵%張雷%鄭應鍵
장의준%여대유%하홍병%장뢰%정응건
瓦斯抽排管%自平衡浮力法下管技术%双塞下管
瓦斯抽排管%自平衡浮力法下管技術%雙塞下管
와사추배관%자평형부역법하관기술%쌍새하관
gas drainage pipe%technology of sinking pipe by self -buoyancy%double-stopper sinking pipe
采用双塞自平衡法下瓦斯抽排管时,上部空管段长度达到了300 m,管内外压力差和提管拉力共同作用,发生瘪管事故。基于此,提出了在上部工作管内用陶粒置换泥浆的下管技术。通过室内试验,测得普通陶粒的抗围压强度为2.4 MPa。当泥浆密度为1200 kg/m3时,对应陶粒放置深度200 m,并分析了普通陶粒的在围压作用下的破坏机理。现场应用表明,用陶粒置换泥浆,明显减轻钻塔负荷;减小了管内外压力差值,有效避免了套管的瘪管事故。
採用雙塞自平衡法下瓦斯抽排管時,上部空管段長度達到瞭300 m,管內外壓力差和提管拉力共同作用,髮生癟管事故。基于此,提齣瞭在上部工作管內用陶粒置換泥漿的下管技術。通過室內試驗,測得普通陶粒的抗圍壓彊度為2.4 MPa。噹泥漿密度為1200 kg/m3時,對應陶粒放置深度200 m,併分析瞭普通陶粒的在圍壓作用下的破壞機理。現場應用錶明,用陶粒置換泥漿,明顯減輕鑽塔負荷;減小瞭管內外壓力差值,有效避免瞭套管的癟管事故。
채용쌍새자평형법하와사추배관시,상부공관단장도체도료300 m,관내외압력차화제관랍력공동작용,발생별관사고。기우차,제출료재상부공작관내용도립치환니장적하관기술。통과실내시험,측득보통도립적항위압강도위2.4 MPa。당니장밀도위1200 kg/m3시,대응도립방치심도200 m,병분석료보통도립적재위압작용하적파배궤리。현장응용표명,용도립치환니장,명현감경찬탑부하;감소료관내외압력차치,유효피면료투관적별관사고。
In the engineering of sinking pipe by double -stopper self -balanced buoyancy method , when the length of top empty pipe reached 300 meters, under the interaction of internal and external pressure difference and tension of lifting pipe , collapse accident occurred .Based on this , a new technology in which mud is re-placed by ceramist in the upper part of the pipe was put forward .In the indoor experiment , the ceramist ’ s strength of resistance against surrounding pressure was measured to be 2.4 MPa, which responding to the depth of 200 m of ceramist placed in the mud , with the density of the mud 1 200 kg/m3 .Failure mechanism of the ce-ramist under the surrounding pressure was analyzed as well .Finally, the field application showed that replacing mud by ceramist obviously reduces the load of rig during sinking pipe and also reduces the difference of internal and external pressure , and the collapse of tube is effectively avoided .