特钢技术
特鋼技術
특강기술
SPECIAL STEEL TECHNOLOGY
2013年
2期
19-22
,共4页
韦佩%南莉%马小菊%杨亚社
韋珮%南莉%馬小菊%楊亞社
위패%남리%마소국%양아사
TA2钛管%氧含量%显微组织%力学性能%成品探伤合格率
TA2鈦管%氧含量%顯微組織%力學性能%成品探傷閤格率
TA2태관%양함량%현미조직%역학성능%성품탐상합격솔
TA2 titanium tube%Oxygen content%Microstructure%Mechanical properties%Flaw detection pass rate of finished product
研究不同氧含量TA2纯钛管材的性能、组织和轧制过程。结果表明,冷加工的TA2管材,在氧含量为0.06%~0.07%时,在500℃时室温力学性能满足飞机发动机要求,组织存在大部分加工组织流线,但当温度达到520℃时显微组织发生完全再结晶,不能满足要求,合格温度区间较窄,不建议选用;在氧含量为0.10%时,在500℃时开始发生再结晶,520℃~600℃热处理时材料组织为细小的再结晶组织,性能和组织趋于稳定,经520℃~550℃×90min FC处理后的管材组织和性能达到飞机发动机使用要求;经过增加内表面镗削处理的方法可以有效的去除氧含量为0.10%的管材在冷加工过程中产生的内表面缺陷,且并不影响成品超声探伤。
研究不同氧含量TA2純鈦管材的性能、組織和軋製過程。結果錶明,冷加工的TA2管材,在氧含量為0.06%~0.07%時,在500℃時室溫力學性能滿足飛機髮動機要求,組織存在大部分加工組織流線,但噹溫度達到520℃時顯微組織髮生完全再結晶,不能滿足要求,閤格溫度區間較窄,不建議選用;在氧含量為0.10%時,在500℃時開始髮生再結晶,520℃~600℃熱處理時材料組織為細小的再結晶組織,性能和組織趨于穩定,經520℃~550℃×90min FC處理後的管材組織和性能達到飛機髮動機使用要求;經過增加內錶麵鏜削處理的方法可以有效的去除氧含量為0.10%的管材在冷加工過程中產生的內錶麵缺陷,且併不影響成品超聲探傷。
연구불동양함량TA2순태관재적성능、조직화알제과정。결과표명,랭가공적TA2관재,재양함량위0.06%~0.07%시,재500℃시실온역학성능만족비궤발동궤요구,조직존재대부분가공조직류선,단당온도체도520℃시현미조직발생완전재결정,불능만족요구,합격온도구간교착,불건의선용;재양함량위0.10%시,재500℃시개시발생재결정,520℃~600℃열처리시재료조직위세소적재결정조직,성능화조직추우은정,경520℃~550℃×90min FC처리후적관재조직화성능체도비궤발동궤사용요구;경과증가내표면당삭처리적방법가이유효적거제양함량위0.10%적관재재랭가공과정중산생적내표면결함,차병불영향성품초성탐상。
In this paper, the performance, structure and rolling process of TA2 titanium pipe with different oxy?gen content were studied.The results showed that when the oxygen content was between 0.06%and 0.07%, the me?chanical properties of the cold-worked TA2 tube met the requirements of aircraft engine at 500℃, and in most micro?structure processed structure flow-line could be seen;when temperature reached 520℃, the microstructure complete?ly recrystallized and the mechanical properties did not meet the requirements, so this narrow temperature range is not recommended;when the oxygen content is 0.10%, recrystallization occurred at 500℃. Fine structure was obtained af?ter heat treatment at 520~600℃and material performance and structure tended to stabilize;After the process of 520~550℃× 90min FC , the performance and structure of the tube met the requirements of aircraft engines;for TA2 tita?nium tube with the oxygen content of 0.10%, the inner surface defects generated in cold working process could be re?moved effectively by boring inner surface, while not affect the ultrasonic flaw detection of finished products.