轴承
軸承
축승
BEARING
2014年
6期
14-17
,共4页
郭明月%楼洪梁%李兴林%姚敏雅%陈炳顺
郭明月%樓洪樑%李興林%姚敏雅%陳炳順
곽명월%루홍량%리흥림%요민아%진병순
滚动轴承%磨削%6σ%圆度误差%正交试验%方差分析
滾動軸承%磨削%6σ%圓度誤差%正交試驗%方差分析
곤동축승%마삭%6σ%원도오차%정교시험%방차분석
rolling-bearing%grinding%sixσ%roundness-error%orthogonal-experiment%variance-analysis
应用6σ方法对轴承套圈磨削工艺进行改进,以轴承外圈圆度误差为评定指标,对磨削工艺中存在的问题进行定义,对外圈圆度误差进行了测量。针对测量结果进行单因素方差分析,得出了工件中心高、导轮倾斜角和磨削砂轮平衡是影响套圈圆度误差的3个主要因素。设计正交试验,分析结果显示,磨削砂轮平衡对圆度误差的影响最大,导轮倾斜角与工件中心高对圆度误差的影响程度相当,低于磨削砂轮平衡对圆度误差的影响。在此基础上提出了对这3个参数进行控制的优化措施,最终使套圈的磨削过程能力指数从0.88提高到了1.43,减少了抽检的次数和数量。
應用6σ方法對軸承套圈磨削工藝進行改進,以軸承外圈圓度誤差為評定指標,對磨削工藝中存在的問題進行定義,對外圈圓度誤差進行瞭測量。針對測量結果進行單因素方差分析,得齣瞭工件中心高、導輪傾斜角和磨削砂輪平衡是影響套圈圓度誤差的3箇主要因素。設計正交試驗,分析結果顯示,磨削砂輪平衡對圓度誤差的影響最大,導輪傾斜角與工件中心高對圓度誤差的影響程度相噹,低于磨削砂輪平衡對圓度誤差的影響。在此基礎上提齣瞭對這3箇參數進行控製的優化措施,最終使套圈的磨削過程能力指數從0.88提高到瞭1.43,減少瞭抽檢的次數和數量。
응용6σ방법대축승투권마삭공예진행개진,이축승외권원도오차위평정지표,대마삭공예중존재적문제진행정의,대외권원도오차진행료측량。침대측량결과진행단인소방차분석,득출료공건중심고、도륜경사각화마삭사륜평형시영향투권원도오차적3개주요인소。설계정교시험,분석결과현시,마삭사륜평형대원도오차적영향최대,도륜경사각여공건중심고대원도오차적영향정도상당,저우마삭사륜평형대원도오차적영향。재차기출상제출료대저3개삼수진행공제적우화조시,최종사투권적마삭과정능력지수종0.88제고도료1.43,감소료추검적차수화수량。
The grinding process for bearing rings is improved by using sixσmethod.The roundness error of outer rings is selected as the assessment index,the existing problems in the grinding process are defined,and the roundness error of outer rings is measured.The measuring results are analyzed by using one-way variance analysis,the workpiece cen-ter height,guide wheel tilt angle and grinding wheel balance are the three main factors that affecting roundness error of rings.The orthogonal experiment is designed.The analysis results show that the grinding wheel balance has the greatest infulence on roundness error,resulting in tilt angle and workpiece center height has the same influence on roundness er-ror,and the influence is less than the influence of grinding wheel balance on roundness error.On this basis,the optimal improvement measure is put forward to control these three parameters.Ultimately,the grinding process capability index is increased from 0.88 to 1.43,the sampling frequency and quantity are reduced.