航空计算技术
航空計算技術
항공계산기술
AERONAUTICAL COMPUTER TECHNIQUE
2014年
3期
36-41
,共6页
廖仲坤%王海飞%张璋%陈果%邵伏勇
廖仲坤%王海飛%張璋%陳果%邵伏勇
료중곤%왕해비%장장%진과%소복용
航空发动机%整机振动%松动故障%故障分析%松动特征
航空髮動機%整機振動%鬆動故障%故障分析%鬆動特徵
항공발동궤%정궤진동%송동고장%고장분석%송동특정
aero-engine%vibration of the whole engine%looseness fault%fault analysis%looseness features
针对某型弹用涡扇发动机振动超标问题,建立了一维有限元梁模型进行仿真与模拟,结合实际试车数据进行了故障分析和仿真,验证了故障原因在于工作转速内存在临界转速,在较大的不平衡力作用下,松动故障被激发。针对机匣加速度信号,研究了不对称刚度模型下松动故障的冲击特征,发现了松动故障所引发的机匣加速度时域波形特征的不对称性以及频谱中出现倍频特征,与实际弹用涡扇发动机试车数据非常一致。结果表明:振动故障是由于支承刚度不足,导致在临界转速附近出现松动故障。
針對某型彈用渦扇髮動機振動超標問題,建立瞭一維有限元樑模型進行倣真與模擬,結閤實際試車數據進行瞭故障分析和倣真,驗證瞭故障原因在于工作轉速內存在臨界轉速,在較大的不平衡力作用下,鬆動故障被激髮。針對機匣加速度信號,研究瞭不對稱剛度模型下鬆動故障的遲擊特徵,髮現瞭鬆動故障所引髮的機匣加速度時域波形特徵的不對稱性以及頻譜中齣現倍頻特徵,與實際彈用渦扇髮動機試車數據非常一緻。結果錶明:振動故障是由于支承剛度不足,導緻在臨界轉速附近齣現鬆動故障。
침대모형탄용와선발동궤진동초표문제,건립료일유유한원량모형진행방진여모의,결합실제시차수거진행료고장분석화방진,험증료고장원인재우공작전속내존재림계전속,재교대적불평형력작용하,송동고장피격발。침대궤갑가속도신호,연구료불대칭강도모형하송동고장적충격특정,발현료송동고장소인발적궤갑가속도시역파형특정적불대칭성이급빈보중출현배빈특정,여실제탄용와선발동궤시차수거비상일치。결과표명:진동고장시유우지승강도불족,도치재림계전속부근출현송동고장。
Certain missile turbofan engine vibration was over standard , so a one-dimensional finite ele-ment beam model was established to simulate .The data from test were combined for fault analysis and simulation ,which was verified that there was critical speed at working speed .Loosen fault would be excit-ed under larger unbalanced force.In this paper ,shock features of asymmetric stiffness model to casing ac-celeration signal were analyzed ,discovering that looseness would lead to asymmetrical features of accelera-tion time domain wave and multiple frequency features of frequency spectrum ,which was consistent with the data from test .Asymmetric stiffness looseness model was verified to be more fit for aeroengine loose-ness fault model .The results show vibration fault is caused by improper support stiffness ,which leads to looseness fault near the critical speed .