化肥工业
化肥工業
화비공업
JOURNAL OF THE CHEMICAL FERTILIZER INDUSTRY
2014年
3期
47-49
,共3页
焦炉气%甲醇%总碳利用率
焦爐氣%甲醇%總碳利用率
초로기%갑순%총탄이용솔
coke-oven gas%methanol%total carbon utilization efficiency
在以焦炉气为原料生产甲醇过程中,新鲜合成气的总碳利用率达不到设计要求,为此采取了调整转化炉工艺操作条件的措施,即提高转化炉温度和压力、降低水碳比等以降低新鲜合成气中 CO2的含量。改进后,催化剂使用后期的精甲醇产量和新鲜合成气的总碳利用率分别提高了19 t/d和9.4%,CO2排放量减少了8623 t/a。
在以焦爐氣為原料生產甲醇過程中,新鮮閤成氣的總碳利用率達不到設計要求,為此採取瞭調整轉化爐工藝操作條件的措施,即提高轉化爐溫度和壓力、降低水碳比等以降低新鮮閤成氣中 CO2的含量。改進後,催化劑使用後期的精甲醇產量和新鮮閤成氣的總碳利用率分彆提高瞭19 t/d和9.4%,CO2排放量減少瞭8623 t/a。
재이초로기위원료생산갑순과정중,신선합성기적총탄이용솔체불도설계요구,위차채취료조정전화로공예조작조건적조시,즉제고전화로온도화압력、강저수탄비등이강저신선합성기중 CO2적함량。개진후,최화제사용후기적정갑순산량화신선합성기적총탄이용솔분별제고료19 t/d화9.4%,CO2배방량감소료8623 t/a。
In the process of making methanol by using coke-oven gas as raw material , total carbon utilization efficiency of fresh synthesis gas is lower than design target , measures are taken thus adjusting working conditions of converter by raising its temperature and pressure , lowering water/carbon ratio to reduce CO 2 in fresh synthesis gas .It has been found the output of purified methanol and total carbon utilization efficiency have been improved by 19 t/d and 9.4% in later service period of catalyst , and CO 2 emission has been reduced about 8 623 t/a.