广西大学学报(自然科学版)
廣西大學學報(自然科學版)
엄서대학학보(자연과학판)
JOURNAL OF GUANGXI UNIVERSITY (NATURAL SCIENCE EDITION)
2014年
4期
894-899
,共6页
风洞试验%节段模型%加劲梁%铁路挑臂%颤振性能
風洞試驗%節段模型%加勁樑%鐵路挑臂%顫振性能
풍동시험%절단모형%가경량%철로도비%전진성능
wind tunnel test%sectional model%stiffening girder%cantilever%flutter stability
为了提高加劲梁的颤振性能,针对某三塔两跨公铁两用悬索桥进行了节段模型风洞试验,探讨了多种气动措施对加劲梁颤振临界风速的影响。结果显示,在三种风攻角下,常规气动措施如增加上下桥面板中央稳定板、铁路道板及检修道开槽等措施降低了加劲梁的颤振临界风速,封闭铁路挑臂并给合上桥面板上、下中央稳定板后,加劲梁在三种风攻角下的颤振性能均大幅提高,使颤振临界风速满足要求。相关结论可为类似桥梁断面的颤振优化提供借鉴。
為瞭提高加勁樑的顫振性能,針對某三塔兩跨公鐵兩用懸索橋進行瞭節段模型風洞試驗,探討瞭多種氣動措施對加勁樑顫振臨界風速的影響。結果顯示,在三種風攻角下,常規氣動措施如增加上下橋麵闆中央穩定闆、鐵路道闆及檢脩道開槽等措施降低瞭加勁樑的顫振臨界風速,封閉鐵路挑臂併給閤上橋麵闆上、下中央穩定闆後,加勁樑在三種風攻角下的顫振性能均大幅提高,使顫振臨界風速滿足要求。相關結論可為類似橋樑斷麵的顫振優化提供藉鑒。
위료제고가경량적전진성능,침대모삼탑량과공철량용현색교진행료절단모형풍동시험,탐토료다충기동조시대가경량전진림계풍속적영향。결과현시,재삼충풍공각하,상규기동조시여증가상하교면판중앙은정판、철로도판급검수도개조등조시강저료가경량적전진림계풍속,봉폐철로도비병급합상교면판상、하중앙은정판후,가경량재삼충풍공각하적전진성능균대폭제고,사전진림계풍속만족요구。상관결론가위유사교량단면적전진우화제공차감。
To improve the flutter stability of stiffened girder, the sectional model wind tunnel tests of a long span highway-railway suspension bridge with two main spans and three towers were carried out. A variety of aerodynamic measures on the flutter stability were explored. The results indicate that conventional aerodynamic measures such as the upper and lower central stabilizer, slotting rail road board and railway maintenance road reduce the critical flutter wind speed in three attack angle cases, while the flutter stability is increased significantly after closing the railway cantilever and u-sing the upper and lower central stabilizer in upper deck, which meets the requirement of standard. The conclusions can provide some references for similar bridge cross-section in the optimization of flutter stability.