石油钻采工艺
石油鑽採工藝
석유찬채공예
OIL DRILLING & PRODUCTION TECHNOLOGY
2014年
5期
28-32
,共5页
肖春学%王向延%姚永永%孙海峰%李清%周君杰
肖春學%王嚮延%姚永永%孫海峰%李清%週君傑
초춘학%왕향연%요영영%손해봉%리청%주군걸
小井眼%钻井%靖南气田
小井眼%鑽井%靖南氣田
소정안%찬정%정남기전
slim hole%drilling%Jingnan Gasifeld
G68-16井是靖南气田区块第1口?206.4 mm小井眼试验井。针对该区块地层复杂地质特征,结合G68-16井小井眼钻井特点,优化钻具组合、优选钻头和螺杆型号,通过参数优化、钻井液性能维护以及预防井下复杂和事故等技术对策,使该井二开钻进4趟钻、划眼4趟钻完钻,钻井后期因处理井下复杂划眼历时16 d,完井作业顺利,平均机械钻速比原?215.9 mm井眼提高了19%。试验取得较好的效果,为该区块进一步进行小井眼钻井试验积累了经验,为提速提供了有利的技术参考。
G68-16井是靖南氣田區塊第1口?206.4 mm小井眼試驗井。針對該區塊地層複雜地質特徵,結閤G68-16井小井眼鑽井特點,優化鑽具組閤、優選鑽頭和螺桿型號,通過參數優化、鑽井液性能維護以及預防井下複雜和事故等技術對策,使該井二開鑽進4趟鑽、劃眼4趟鑽完鑽,鑽井後期因處理井下複雜劃眼歷時16 d,完井作業順利,平均機械鑽速比原?215.9 mm井眼提高瞭19%。試驗取得較好的效果,為該區塊進一步進行小井眼鑽井試驗積纍瞭經驗,為提速提供瞭有利的技術參攷。
G68-16정시정남기전구괴제1구?206.4 mm소정안시험정。침대해구괴지층복잡지질특정,결합G68-16정소정안찬정특점,우화찬구조합、우선찬두화라간형호,통과삼수우화、찬정액성능유호이급예방정하복잡화사고등기술대책,사해정이개찬진4쟁찬、화안4쟁찬완찬,찬정후기인처리정하복잡화안력시16 d,완정작업순리,평균궤계찬속비원?215.9 mm정안제고료19%。시험취득교호적효과,위해구괴진일보진행소정안찬정시험적루료경험,위제속제공료유리적기술삼고。
Well G68-16 is the ifrst test well for ?206.4 mm slim hole in the south of Jingbian gas ifeld block. In line with complex formation characteristics in this block and combining drilling characteristics of G68-16 slim hole, optimizing bottom hole assembly (BHA), drill bit and screw model, technical measures like optimizing the parameters, drilling lfuid maintenance and prevention of down-hole troubles were applied, The well was successfully drilled with four runs during the second section and four runs for reaming;reaming down took 16 days due to handling downhole trouble in later drilling stage;the average penetration rate was increased by 19%compared with the original ?215.9 mm hole. The test is very successful, has accumulated experience for further slim hole test drilling in this block and provides favorable technical reference for increasing drilling rate.