地震工程学报
地震工程學報
지진공정학보
China Earthquake Engineering Journal
2014年
3期
462-467
,共6页
李飒%王耀存%蒲玉成%孙振平%樊之夏%韩亮
李颯%王耀存%蒲玉成%孫振平%樊之夏%韓亮
리삽%왕요존%포옥성%손진평%번지하%한량
溜桩%打桩记录%动测%承载力
霤樁%打樁記錄%動測%承載力
류장%타장기록%동측%승재력
pile sinking%pile driving records%dynamic load test%pile capacity
打桩过程中突然快速的溜桩可能造成脱锤,桩体破坏,引发安全事故。由于溜桩的产生往往造成打桩锤击数的预测值与实测值具有较大的偏差,此时准确评价溜桩后桩基承载力就成为实际工程中非常关注的问题。本文选择我国东海两个工程实例,根据现场高应变动测试验和打桩记录,研究了溜桩对桩基承载力的影响。计算分析显示,溜桩的产生会导致打桩总能量的明显降低;现场动测试验结果显示,溜桩发生后在发生溜桩的土层的桩体侧摩阻力接近于零,而桩端阻力没有明显的异常,说明溜桩导致的承载力降低主要来自于侧摩阻力的减小。在本文的实例中,溜桩导致的桩基承载力的降低最大可以达到桩基承载力计算值的17%。
打樁過程中突然快速的霤樁可能造成脫錘,樁體破壞,引髮安全事故。由于霤樁的產生往往造成打樁錘擊數的預測值與實測值具有較大的偏差,此時準確評價霤樁後樁基承載力就成為實際工程中非常關註的問題。本文選擇我國東海兩箇工程實例,根據現場高應變動測試驗和打樁記錄,研究瞭霤樁對樁基承載力的影響。計算分析顯示,霤樁的產生會導緻打樁總能量的明顯降低;現場動測試驗結果顯示,霤樁髮生後在髮生霤樁的土層的樁體側摩阻力接近于零,而樁耑阻力沒有明顯的異常,說明霤樁導緻的承載力降低主要來自于側摩阻力的減小。在本文的實例中,霤樁導緻的樁基承載力的降低最大可以達到樁基承載力計算值的17%。
타장과정중돌연쾌속적류장가능조성탈추,장체파배,인발안전사고。유우류장적산생왕왕조성타장추격수적예측치여실측치구유교대적편차,차시준학평개류장후장기승재력취성위실제공정중비상관주적문제。본문선택아국동해량개공정실례,근거현장고응변동측시험화타장기록,연구료류장대장기승재력적영향。계산분석현시,류장적산생회도치타장총능량적명현강저;현장동측시험결과현시,류장발생후재발생류장적토층적장체측마조력접근우령,이장단조력몰유명현적이상,설명류장도치적승재력강저주요래자우측마조력적감소。재본문적실례중,류장도치적장기승재력적강저최대가이체도장기승재력계산치적17%。
Pile sinking during pile driving is common.A sudden drop of a pile after a strike from the hammer may cause a serious accident,such as the pile falling out of the drive cap or damage to the pile from high tension stress.Pile sinking also often causes a large deviation between the drivabili-ty prediction and the measured blow count.Therefore,an accurate assessment of pile capacity af-ter pile sinking becomes an important problem to address in practice.In this paper,two projects in the East China Sea are chosen to analyze.Based on the results of dynamic load tests in the field and pile driving records,the influence of pile sinking on pile capacity at the end of driving (EOD) is studied.The analysis results show that pile sinking will lead to a significant decrease in the total energy used in pile driving.The results from CAPWAP show that the unit friction of a soil layer where piles run off is close to zero,while the pile end resistance shows no obvious abnormalities. This indicates that the decrease in pile capacity caused by pile sinking is mainly from friction re-duction.In this instance,the pile capacity reduction resulting from pile sinking can reach a maxi-mum of 17% of the designed value.