湖南电力
湖南電力
호남전력
HUNAN ELECTRIC POWER
2014年
5期
26-28,31
,共4页
上导摆度%在线监测%变转速%变励磁%变负荷
上導襬度%在線鑑測%變轉速%變勵磁%變負荷
상도파도%재선감측%변전속%변려자%변부하
upper guide throw%online monitoring%variable speed%variable excitation%variable load
针对五强溪水电厂5号机组上导摆度偏大问题,利用机组稳定性在线监测系统的录波、计算、分析功能,实施机组的变转速、变励磁、变负荷试验,采用多种方法进行分析,得出发电机转子质量不平衡是导致5号机组摆度偏大的主要原因的结论。
針對五彊溪水電廠5號機組上導襬度偏大問題,利用機組穩定性在線鑑測繫統的錄波、計算、分析功能,實施機組的變轉速、變勵磁、變負荷試驗,採用多種方法進行分析,得齣髮電機轉子質量不平衡是導緻5號機組襬度偏大的主要原因的結論。
침대오강계수전엄5호궤조상도파도편대문제,이용궤조은정성재선감측계통적록파、계산、분석공능,실시궤조적변전속、변려자、변부하시험,채용다충방법진행분석,득출발전궤전자질량불평형시도치5호궤조파도편대적주요원인적결론。
Aiming to large numerical value of upper guide throw for Wuqiangxi Hydropower Plant NO. 5 unit, several stability tests including variable speed test, variable excitation test and variable load test are independently designed and implemented by making use of the recording, calculation, analysis function of hydropower unit stability online monitoring system by a variety of methods. Through the above measures, the conclusion are drawn that the generator rotor mass imbalance is the main reason of large numerical value of upper guide throw for NO. 5 unit.