农业工程学报
農業工程學報
농업공정학보
2013年
9期
256-266
,共11页
陈建行%刘鹭%孙颜君%苏燕玲%张书文%孔凡丕%蒋士龙%吕加平
陳建行%劉鷺%孫顏君%囌燕玲%張書文%孔凡丕%蔣士龍%呂加平
진건행%류로%손안군%소연령%장서문%공범비%장사룡%려가평
膜%分离%过滤%酪蛋白胶束粉%陶瓷膜
膜%分離%過濾%酪蛋白膠束粉%陶瓷膜
막%분리%과려%락단백효속분%도자막
membranes%separation%filtration%micellar casein concentrate%ceramic membrane
为尽快建立酪蛋白胶束粉(micellar casein concentrate, MCC)的中试生产线,实现MCC在国内的工业化生产,该研究通过测定牛乳蛋白粒径,选取孔径40和100 nm的中空纤维陶瓷膜进行膜分离效果的对比,并选用膜分离效果较佳的陶瓷膜进行最佳操作参数的确定及稀释过滤工艺的研究,最后将自制MCC和进口MCC进行品质特性对比并分析其工业化生产的可能性.结果表明:孔径40 nm中空纤维陶瓷膜与孔径100 nm中空纤维陶瓷膜相比,渗透液中不含酪蛋白,能够减少酪蛋白损失,更适合于酪蛋白和乳清蛋白的分离,孔径40nm中空纤维陶瓷膜的最佳操作参数为操作压力2×105 Pa,料液温度50℃;采用四段式的连续稀释过滤工艺,可使料液中酪蛋白占真蛋白的比例从69.39%提升至93.34%,真蛋白占干物质的比例从38.45%提升至88.15%;稀释过滤完毕后膜的纯水通量衰减了39.98%,经生物酶清洗液清洗后膜的纯水通量恢复至初始的98.02%;自制MCC在成分组成上与加拿大Proteinco公司生产的MCC相比差异不显著(p<0.05),但在溶解度和粉粒的微观形态上优于Proteinco MCC;生产1 kg MCC需要原料乳46.24 L,成本为244.58元,可实现其国内工业化生产.研究结果为实现MCC在国内工业化生产及其应用性研究提供参考.
為儘快建立酪蛋白膠束粉(micellar casein concentrate, MCC)的中試生產線,實現MCC在國內的工業化生產,該研究通過測定牛乳蛋白粒徑,選取孔徑40和100 nm的中空纖維陶瓷膜進行膜分離效果的對比,併選用膜分離效果較佳的陶瓷膜進行最佳操作參數的確定及稀釋過濾工藝的研究,最後將自製MCC和進口MCC進行品質特性對比併分析其工業化生產的可能性.結果錶明:孔徑40 nm中空纖維陶瓷膜與孔徑100 nm中空纖維陶瓷膜相比,滲透液中不含酪蛋白,能夠減少酪蛋白損失,更適閤于酪蛋白和乳清蛋白的分離,孔徑40nm中空纖維陶瓷膜的最佳操作參數為操作壓力2×105 Pa,料液溫度50℃;採用四段式的連續稀釋過濾工藝,可使料液中酪蛋白佔真蛋白的比例從69.39%提升至93.34%,真蛋白佔榦物質的比例從38.45%提升至88.15%;稀釋過濾完畢後膜的純水通量衰減瞭39.98%,經生物酶清洗液清洗後膜的純水通量恢複至初始的98.02%;自製MCC在成分組成上與加拿大Proteinco公司生產的MCC相比差異不顯著(p<0.05),但在溶解度和粉粒的微觀形態上優于Proteinco MCC;生產1 kg MCC需要原料乳46.24 L,成本為244.58元,可實現其國內工業化生產.研究結果為實現MCC在國內工業化生產及其應用性研究提供參攷.
위진쾌건립락단백효속분(micellar casein concentrate, MCC)적중시생산선,실현MCC재국내적공업화생산,해연구통과측정우유단백립경,선취공경40화100 nm적중공섬유도자막진행막분리효과적대비,병선용막분리효과교가적도자막진행최가조작삼수적학정급희석과려공예적연구,최후장자제MCC화진구MCC진행품질특성대비병분석기공업화생산적가능성.결과표명:공경40 nm중공섬유도자막여공경100 nm중공섬유도자막상비,삼투액중불함락단백,능구감소락단백손실,경괄합우락단백화유청단백적분리,공경40nm중공섬유도자막적최가조작삼수위조작압력2×105 Pa,료액온도50℃;채용사단식적련속희석과려공예,가사료액중락단백점진단백적비례종69.39%제승지93.34%,진단백점간물질적비례종38.45%제승지88.15%;희석과려완필후막적순수통량쇠감료39.98%,경생물매청세액청세후막적순수통량회복지초시적98.02%;자제MCC재성분조성상여가나대Proteinco공사생산적MCC상비차이불현저(p<0.05),단재용해도화분립적미관형태상우우Proteinco MCC;생산1 kg MCC수요원료유46.24 L,성본위244.58원,가실현기국내공업화생산.연구결과위실현MCC재국내공업화생산급기응용성연구제공삼고.
Micellar casein concentrate (MCC) powder, a new milk protein product produced by a combination of processes including membrane separation, evaporation and spray drying has potential applications in cheese making, whipped topping, coffee whitener and yogurt making. It is becoming more and more popular in the food processing industry, but currently China depends on imported MCC mainly from developed countries. The main objective of this study was to successfully develop a pilot scale production process for micellar casein concentrate powder and facilitate its rapid adoption and manufacturing in China’s dairy plants. Preliminary studies involved the selection of a suitable hollow fiber ceramic membrane for the separation of casein micellar and serum protein between 100 nm and 40 nm pore size hollow fiber ceramic membranes (InoCep, Hyflux Ltd, Singapore). The 40nm pore size hollow fiber ceramic membrane, which had better separation performance, was chosen for further investigation on optimum operating parameters, mainly temperature and pressure. A four-stage diafiltration process was employed, in which chemical composition and flux changes were measured at the end of every stage in the production line. Finally, the micellar casein concentrate powder made after evaporation and spray drying process was compared with commercial MCC (Proteinco Inc., Quebec, Canada) in terms of their physical characteristics and chemical compositions. The yield rate and the production costs were also calculated. The results showed that:(1) the permeate of 100 nm pore size membrane was cloudy but the permeate of 40 nm pore size membrane was clear in appearance and the proportion of casein in the true protein of the permeate for the 100 and 40 nm pore size membrane were 40.03%and 17.48%, respectively. Therefore, the 40nm pore size membrane was found to be more suitable for the separation of casein micellar and serum protein and its average permeate flux during a 3×concentration at the optimal operating conditions (temperature 50℃, pressure 2×105 Pa) was above 60 L/(m2·h);(2) the best time for adding water during the whole diafiltration process was when the volume concentration factor was equal to 3, which reduced membrane fouling and enhanced average stage flux. After four stages of the continuous diafiltration process, the casein micellar purity and the pure protein content (on a dry basis) reached 93.34%and 88.15%, respectively;(3) at the end of the diafiltration process, the water flux declined by 39.98%, and when a biological-enzyme cleaning agent was used, water flux recovery was 98.02%of the initial;(4) The solubility of the pilot scale produced MCC was significantly different from that of the commercial MCC. The solubility was better in the pilot scale produced than commercial MCC, which may be due to the difference of the inlet temperature of spray drying. Additionally, the particle morphologies of the pilot scale-produced MCC, as observed by a scanning electron microscope, appeared spherical and smaller in size, whereas the commercial MCC had wrinkled particle surfaces and large particle sizes. (5) From the chemical analyses, determinations of total solids, lactose, minerals, total protein, true protein, casein protein and serum protein content were done but there were no significant differences (p<0.05) between the pilot scale produced and the commercial MCC. (6) In order to produce 1 kg MCC, 46.24 L raw milk was required and the production cost of MCC was calculated as 244.58 Yuan/kg, which was deemed profitable and therefore can be transformed to the industrialized production stage. The methods and data stated in this study are valuable and useful to the industry and as a benchmark for further studies. They can also be used both as a reference and guide for MCC production in China.