当代化工
噹代化工
당대화공
CONTEMPORARY CHEMICAL INDUSTRY
2012年
12期
1385-1387
,共3页
抽余油%正己烷%加氢%工艺技术%质量优良%效益
抽餘油%正己烷%加氫%工藝技術%質量優良%效益
추여유%정기완%가경%공예기술%질량우량%효익
Raffinate%Hexane%Hydrogenation%Technology%Good quality%Benefit
介绍在中国石油克拉玛依石化公司以重整装置来的抽余油内(含己烷15%~36%)为原料采用精馏分离,除去轻重组分后,得含正己烷纯度为70%~80%馏分.经过705型催化剂加氢脱烯烃,脱除硫、氮等杂质后,再经过MH-6A催化剂苯加氢,除去苯等不饱和烃,得合格正己烷.该工艺技术具有催化剂活性高,寿命长,无需再生,反应条件温和工艺流程简单,产品升值高等特点,成功解决了低辛烷值的抽余油出路问题.同时生产的正己烷产品质量优良,达到了国外同类产品的水平,直接经济效益显著.
介紹在中國石油剋拉瑪依石化公司以重整裝置來的抽餘油內(含己烷15%~36%)為原料採用精餾分離,除去輕重組分後,得含正己烷純度為70%~80%餾分.經過705型催化劑加氫脫烯烴,脫除硫、氮等雜質後,再經過MH-6A催化劑苯加氫,除去苯等不飽和烴,得閤格正己烷.該工藝技術具有催化劑活性高,壽命長,無需再生,反應條件溫和工藝流程簡單,產品升值高等特點,成功解決瞭低辛烷值的抽餘油齣路問題.同時生產的正己烷產品質量優良,達到瞭國外同類產品的水平,直接經濟效益顯著.
개소재중국석유극랍마의석화공사이중정장치래적추여유내(함기완15%~36%)위원료채용정류분리,제거경중조분후,득함정기완순도위70%~80%류분.경과705형최화제가경탈희경,탈제류、담등잡질후,재경과MH-6A최화제분가경,제거분등불포화경,득합격정기완.해공예기술구유최화제활성고,수명장,무수재생,반응조건온화공예류정간단,산품승치고등특점,성공해결료저신완치적추여유출로문제.동시생산적정기완산품질량우량,체도료국외동류산품적수평,직접경제효익현저.
In Karamay petrochemical company, reformate raffinate (hexane content 15%~36%) is used as raw material to produce n-hexane. Firstly, the distillation separation of reformate raffinate is carried out to gain the fraction (n-hexane content 70%~80%),then 705 hydrogenation catalyst is used to remove impurities such as sulfur and nitrogen, and MH-6A benzene hydrogenation catalyst is used to remove saturated hydrocarbons, finally qualified n-hexane is gained. This technology has high catalytic activity, long service life without regeneration, mild reaction conditions, simple process and high product appreciation. At the same time, produced n-hexane has good quality, reaches to the level of the same product at abroad;the direct economic benefit is remarkable.