山东冶金
山東冶金
산동야금
SHANDONG METALLURY
2013年
1期
24-26
,共3页
杨建%林文兵%何航%彭杨
楊建%林文兵%何航%彭楊
양건%림문병%하항%팽양
特厚钢板%探伤合格率%工艺优化%夹杂物%偏析
特厚鋼闆%探傷閤格率%工藝優化%夾雜物%偏析
특후강판%탐상합격솔%공예우화%협잡물%편석
ultra heavy plate%flaw detection qualified rate%process optimization%inclusion%segregation
采用低倍热酸洗、金相、扫描电镜和能谱等方法对特厚板探伤不合格原因进行分析,结果表明,主要原因是钢板中存在大尺寸(20~50μm)钙铝酸盐夹杂物、链状的硫化物夹杂物以及Mn偏析导致的裂纹.通过优化LF炉渣系、VD和LF炉的吹氩制度以及连铸工艺参数,提高了钢水纯净度和板坯质量,钢水中的[P]≤0.015%、[S]≤0.003%、[O]≤4×10-6、[H]≤1.5×10-6、[N]≤35×10-6,板坯的中心偏析和疏松均降为C类1.0级以下,钢板平均探伤合格率提高到了98.8%.
採用低倍熱痠洗、金相、掃描電鏡和能譜等方法對特厚闆探傷不閤格原因進行分析,結果錶明,主要原因是鋼闆中存在大呎吋(20~50μm)鈣鋁痠鹽夾雜物、鏈狀的硫化物夾雜物以及Mn偏析導緻的裂紋.通過優化LF爐渣繫、VD和LF爐的吹氬製度以及連鑄工藝參數,提高瞭鋼水純淨度和闆坯質量,鋼水中的[P]≤0.015%、[S]≤0.003%、[O]≤4×10-6、[H]≤1.5×10-6、[N]≤35×10-6,闆坯的中心偏析和疏鬆均降為C類1.0級以下,鋼闆平均探傷閤格率提高到瞭98.8%.
채용저배열산세、금상、소묘전경화능보등방법대특후판탐상불합격원인진행분석,결과표명,주요원인시강판중존재대척촌(20~50μm)개려산염협잡물、련상적류화물협잡물이급Mn편석도치적렬문.통과우화LF로사계、VD화LF로적취아제도이급련주공예삼수,제고료강수순정도화판배질량,강수중적[P]≤0.015%、[S]≤0.003%、[O]≤4×10-6、[H]≤1.5×10-6、[N]≤35×10-6,판배적중심편석화소송균강위C류1.0급이하,강판평균탐상합격솔제고도료98.8%.
The causes of ultrasonic inspection disqualification for ultra heavy plate were analyzed by means of macroscopic test, metallographic inspection, SEM and EDAX. The results showed that main reasons of ultrasonic test defects are big size of calcium-aluminates inclusions, chain-shaped sulfides inclusion and the crack caused by Mn segregation in the plate. In order to increase the purity of molten liquid steel and improving quality of slab, LF refining slag system was selected, the blowing argon processing of LF and VD was adjusted and the process parameters of casting were optimized. After optimizing,[P]<0.015%,[S]<0.003%,[O]<4×10-6,[H]<1.5×10-6 and[N]<35×10-6. The center segregation and central poriness of slab were less than 1.0 level of C grade. The average qualified ratio of ultrasonic flaw detection is up to 98.8%.