电子测试
電子測試
전자측시
ELECTRONIC TEST
2013年
9期
286-288
,共3页
调剖剂%井组%整体调剖
調剖劑%井組%整體調剖
조부제%정조%정체조부
Profile controlling agent%well group%whole block profile control
针对南翼山油田I+II油层组部分井组高含水的状况,为了提高注入水的波及体积和驱油效率,开展了调剖堵水作业.利用筛选出的调剖剂体系,对井组进行优选,选择有代表性的南浅734井组进行先导性实验.现场施工表明,筛选的调剖剂适应性强,施工后井组含水下降,产油量上升,取得了巨大的经济效益,达到了预期目的.建议推广区块整体调剖措施,实现油田的高产稳产.
針對南翼山油田I+II油層組部分井組高含水的狀況,為瞭提高註入水的波及體積和驅油效率,開展瞭調剖堵水作業.利用篩選齣的調剖劑體繫,對井組進行優選,選擇有代錶性的南淺734井組進行先導性實驗.現場施工錶明,篩選的調剖劑適應性彊,施工後井組含水下降,產油量上升,取得瞭巨大的經濟效益,達到瞭預期目的.建議推廣區塊整體調剖措施,實現油田的高產穩產.
침대남익산유전I+II유층조부분정조고함수적상황,위료제고주입수적파급체적화구유효솔,개전료조부도수작업.이용사선출적조부제체계,대정조진행우선,선택유대표성적남천734정조진행선도성실험.현장시공표명,사선적조부제괄응성강,시공후정조함수하강,산유량상승,취득료거대적경제효익,체도료예기목적.건의추엄구괴정체조부조시,실현유전적고산은산.
In the situation of high water with part of well group in I+II oil group of the Nanyishan oilfield,in order to improve water injection volume and displacement efficiency,the profile control and water shutoff operations wan taken in 2012. The construction site showed that profile control agent had good adaptability,the water of well group dropped and oil production increased after the construction. The construction made great economic benefits,to achieve the expected goal. Recommendation was that it should promote the whole block profile control measures for high and stable production of the oilfield.