石油与天然气化工
石油與天然氣化工
석유여천연기화공
CHEMICAL ENGINEERING OF OIL AND GAS
2015年
1期
75-78
,共4页
聂岚%袁宗明%杨锦林%青成凤%周永淳
聶嵐%袁宗明%楊錦林%青成鳳%週永淳
섭람%원종명%양금림%청성봉%주영순
川西气田%排水采气%泡排剂%泡沫%消泡剂%气液分离效率%现场试验%效果评价
川西氣田%排水採氣%泡排劑%泡沫%消泡劑%氣液分離效率%現場試驗%效果評價
천서기전%배수채기%포배제%포말%소포제%기액분리효솔%현장시험%효과평개
western Sichuan gas field%drainage gas production%foaming agent%foam%defoamer%gas-liquid separation efficiency%field test%effect evaluation
针对目前液体消泡剂使用的局限性,川西气田引进了XXP‐1固体消泡剂,在含泡沫液天然气进入分离器之前消除其携带的泡沫。在X5、XC6和XY H F‐2井进行了现场试验。试验结果表明, XXP‐1固体消泡剂对X5、XC6和XY HF‐2气井水样具有较好的破泡、抑泡能力,平均破泡时间小于10 s ,平均抑泡时间大于6 min。加注XXP‐1固体消泡剂后,污水罐泡沫高度明显下降,站场月污水拉运量大大提高,天然气出站压力降低,接近管网压力。XXP‐1固体消泡剂能有效消除携液天然气中的泡沫,提高分离器气液分离效率。
針對目前液體消泡劑使用的跼限性,川西氣田引進瞭XXP‐1固體消泡劑,在含泡沫液天然氣進入分離器之前消除其攜帶的泡沫。在X5、XC6和XY H F‐2井進行瞭現場試驗。試驗結果錶明, XXP‐1固體消泡劑對X5、XC6和XY HF‐2氣井水樣具有較好的破泡、抑泡能力,平均破泡時間小于10 s ,平均抑泡時間大于6 min。加註XXP‐1固體消泡劑後,汙水罐泡沫高度明顯下降,站場月汙水拉運量大大提高,天然氣齣站壓力降低,接近管網壓力。XXP‐1固體消泡劑能有效消除攜液天然氣中的泡沫,提高分離器氣液分離效率。
침대목전액체소포제사용적국한성,천서기전인진료XXP‐1고체소포제,재함포말액천연기진입분리기지전소제기휴대적포말。재X5、XC6화XY H F‐2정진행료현장시험。시험결과표명, XXP‐1고체소포제대X5、XC6화XY HF‐2기정수양구유교호적파포、억포능력,평균파포시간소우10 s ,평균억포시간대우6 min。가주XXP‐1고체소포제후,오수관포말고도명현하강,참장월오수랍운량대대제고,천연기출참압력강저,접근관망압력。XXP‐1고체소포제능유효소제휴액천연기중적포말,제고분리기기액분리효솔。
Aiming at the application restriction of liquid defoaming agent ,XXP‐1 solid defoaming agent was introduced and field tests were conducted in X5 ,XC6 and XYHF‐2 gas wells of the western Sichuan gas field .T he results indicated that XXP‐1 solid defoamer has good capacity of breaking bub‐bles and inhibiting foam generation ,the defoaming time of XXP‐1 solid defoaming agent was less than 10 s and the inhibiting time was more than 6 min .The height of foam in sewage tank substantially re‐duced ,monthly sewage pull capacity of upstream well station was greatly increased ,and the gas out‐let pressure dropped and approached to the pressure of pipe network after injecting XXP‐1 solid de‐foamer .XXP‐1 solid defoaming agent could efficiently eliminate the bubble and improve the gas‐liquid separation efficiency .