水力发电
水力髮電
수력발전
WATER POWER
2015年
2期
90-93
,共4页
水力学%岸边溢洪道%明渠溢洪道%双泄中孔%观音岩水电站
水力學%岸邊溢洪道%明渠溢洪道%雙洩中孔%觀音巖水電站
수역학%안변일홍도%명거일홍도%쌍설중공%관음암수전참
hydraulics%river-bank spillway%open channel spillway%double discharge middle outlet%Guanyinyan Hydropower Station
结合观音岩水电站泄水建筑物的关键水力学问题,阐述了双泄中孔掺气减蚀试验、明渠溢流坝消力池体形优化试验、岸边溢洪道取消中隔墙试验的研究成果。研究结果表明:双泄中孔泄槽底板掺气减蚀效果总体较好;明渠溢流坝新型跌坎渐扩式消力池消能充分,临底水力学参数较小,应加强底板关键区域的结构稳定设计;岸边溢洪道取消中隔墙后基本不影响下游河道的消能防冲效果,但是减弱了工程运行的灵活性,运行宜同时参照工程调度试验成果。
結閤觀音巖水電站洩水建築物的關鍵水力學問題,闡述瞭雙洩中孔摻氣減蝕試驗、明渠溢流壩消力池體形優化試驗、岸邊溢洪道取消中隔牆試驗的研究成果。研究結果錶明:雙洩中孔洩槽底闆摻氣減蝕效果總體較好;明渠溢流壩新型跌坎漸擴式消力池消能充分,臨底水力學參數較小,應加彊底闆關鍵區域的結構穩定設計;岸邊溢洪道取消中隔牆後基本不影響下遊河道的消能防遲效果,但是減弱瞭工程運行的靈活性,運行宜同時參照工程調度試驗成果。
결합관음암수전참설수건축물적관건수역학문제,천술료쌍설중공참기감식시험、명거일류패소력지체형우화시험、안변일홍도취소중격장시험적연구성과。연구결과표명:쌍설중공설조저판참기감식효과총체교호;명거일류패신형질감점확식소력지소능충분,림저수역학삼수교소,응가강저판관건구역적결구은정설계;안변일홍도취소중격장후기본불영향하유하도적소능방충효과,단시감약료공정운행적령활성,운행의동시삼조공정조도시험성과。
The key hydraulic problems for the water discharge structure of Guanyinyan Hydropower Station are studied by experiments, including aeration and cavitation prevention test of double discharge middle outlets, stilling basin shape optimization test for the open channel spillway and canceling mid-partition test for river-bank spillway. The result shows that, (a) the aeration effect for cavitation prevention of chute bottom of double discharge middle outlets is good; (b) the stilling basin with step-down and diffuser in the channel spillway can fully dissipate energy, the hydraulic parameters near the bottom are smaller, but the structural stability design of key areas in the floor should be improved;and (c) the canceling of mid-partition for river-bank spillway nearly does not affect the effect of energy dissipation and erosion resistance of downstream river channel, but the operation flexibility of station will be weakened which should be optimized according to operation scheduling test results.